QFR No - 8000854740
Defect Details
NC No. 8000854740
NC Date 12/12/2023
NC Submission Date
Part No. B2SU01002O
Part Name BRAKE HOSE TUBE CLAMP 2 (N282)
Supplier Name & Code 100151-EXCELL PRESSINGS
ETL Plant 1120-ETL K-226/2 Disc Brakes
Defect Details OTHER-BENDING NOT OK
 
1. Problem Description
Defect Description BENDING NOT OK
Detection Stage Inprocess
Problem Severity Fitment
NG Quantity 393
Is Defect Repeatative? No
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID excellpressings.qc@gmail.com
Plant Head/CEO Email ID yogesh_vaidya42@yahoo.co.in
MD Email ID excellpressings@gmail.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
4000
0
0
3000
2000
9000
Check Qty
4000
0
0
3000
2000
9000
NG Qty
393
0
0
0
0
393
 
Scrap 393
Rework 0
Under Deviation 0
Containment Action
100% inspection is done at ETL end and our end also
 
3. Process Flow
Process Flow Description
Blanking& piercing- Z bending- Lug bending- U bending- Final Forming
 
4. Process Details
Process / Operation press operation
Outsource No
Machine / Cell EP-04
Machine / Cell No. EP-04
5. Problem Analysis
Type Possible Cause Fact Verification Jud
ToolOld location pin was wear outDue to wear out location pin, ,movement took place of part on dieO
 
6. Inspection Method Analysis (Current)
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size 10
7. Root Cause Analysis (Occurance)
Why 1 Hole not macthed after full closing at ETL end
Why 2 In U bending operations, movement took place
Why 3 location pin was wear out
Why 4 New operator was on machine at U Bending operations
Why 5 That operator was not aware about the location pin wear out
Root Cause (Occurance) In U bending operation, shifting took place due to location pin wear out
 
Root Cause Analysis (Outflow)
Why 1 Full closing operation is take place at ETL end
Why 2 Partial closing at our end, cant check every job by doing full closing at our end
Why 3
Why 4
Why 5
Root Cause (Outflow) Every job full closing cant be done at our end, as we have to supply partial closing job.
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceNew location pin will be provided, so that movement cant be take placeNikhil Ghodmare & Ankosh Mathure20/12/202320/12/2023Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details Sampling of folding jobs at our end will be increased
Inspection Method Other
Other Inspection Method Rod & block
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size 10
10. Evidance of Countermeasure
Occurance (Before) location pin wear out
614_Occurance_Before.jpg
Occurance (After) old location pin changed and new one added
614_Occurance_After.jpg
Outflow (Before) Hole not meet after full closing at ETL end
614_Outflow_Before.jpg
Outflow (After) Hole meet after full closing
614_Outflow_After.jpg
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant At Excell pressings, hole should be matched after full closing
 
12. Document Review
Documents PMCheckSheet, JHCheckSheet, InspCheckSheet
Specify Other Document FFPA checksheet
 
13. Effectiveness Of Action
Reviewed Quantity 100
Reason for submission No defect found in latest lot