QFR No - 8000854744
Defect Details
NC No. 8000854744
NC Date 12/12/2023
NC Submission Date
Part No. B2SU00702O
Part Name BRAKE HOSE TUBE CLAMP 1(NTORQ)
Supplier Name & Code 100151-EXCELL PRESSINGS
ETL Plant 1120-ETL K-226/2 Disc Brakes
Defect Details PLATING NOT OK-PLATING NOT OK
 
1. Problem Description
Defect Description PLATING NOT OK-PLATING NOT OK
Detection Stage Receipt
Problem Severity Aesthetic
NG Quantity 164
Is Defect Repeatative? Yes
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID excellpressings.qc@gmail.com
Plant Head/CEO Email ID yogesh_vaidya42@gmail.com
MD Email ID excellpressings@gmail.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
1000
0
0
2000
1000
4000
Check Qty
1000
0
0
2000
1000
4000
NG Qty
164
0
0
0
0
164
 
Scrap 0
Rework 164
Under Deviation 0
Containment Action
All the lots are checked at ETL end and our end.
 
3. Process Flow
Process Flow Description
After pressings operation, the material is given for plating to M/S Krishna Industries.Then at final inspection 100% visual inspection is being carried out.
 
4. Process Details
Process / Operation Plating operation
Outsource Yes
Machine / Cell KI _ WATT TANK NO 02
Machine / Cell No. KI _ WATT TANK NO 02
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MethodCurrent supply issue on jigsRectifier wires loose contact so that causes for current fluctuationsO
 
6. Inspection Method Analysis (Current)
Inspection Method Instrument
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size 10
7. Root Cause Analysis (Occurance)
Why 1 Thickness observed below 8 micron
Why 2 Current fluctuations observed
Why 3 Jigs copper getting hot
Why 4 V block getting loosed
Why 5 Monthly maintenance was not done to V block
Root Cause (Occurance) Current fluctuation due to over heat cathode contacts
 
Root Cause Analysis (Outflow)
Why 1 Visul found ok
Why 2 Thickness was not checked
Why 3
Why 4
Why 5
Root Cause (Outflow) Thickness was not checked after plating operation
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceCurrent supply issue caused to lower the thicknessM/S Krishna Industries19/12/202320/12/2023Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details Every lot thickness will be checked at Krishna Industries and Excell pressings
Inspection Method Instrument
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 10
10. Evidance of Countermeasure
Occurance (Before) V block get damaged
616_Occurance_Before.jpg
Occurance (After) V block repaired
616_Occurance_After.jpg
Outflow (Before) Not Ok plating part
616_Outflow_Before.jpg
Outflow (After) Ok plating part
616_Outflow_After.jpg
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant At Krishna Industries, process flow chart is followed on every stage
 
12. Document Review
Documents ControlPlan, JHCheckSheet, InspCheckSheet
Specify Other Document FFPA checksheet
 
13. Effectiveness Of Action
Reviewed Quantity 100
Reason for submission No defect found in latest lot