QFR No - 8000858053
Defect Details
NC No. 8000858053
NC Date 08/01/2024
NC Submission Date
Part No. 550DZ03302
Part Name FORK BOLT
Supplier Name & Code 100189-SANGKAJ STEEL PVT LTD.
ETL Plant 1117-ETL K-228/9 Suspension
Defect Details NOT AS PER SPECIFICATION-M10 THREAD LENGTH UNDERSIZE OBSERVED VAL
 
1. Problem Description
Defect Description M10 thread length undersize
Detection Stage Receipt
Problem Severity Fitment
NG Quantity 1360
Is Defect Repeatative? No
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID qualityassurance@sangkaj.com
Plant Head/CEO Email ID steel@sangkaj.com
MD Email ID anirudh.2007@hotmail.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
0
0
0
1000
0
1000
Check Qty
0
0
0
1000
0
1000
NG Qty
0
0
0
7
0
7
 
Scrap 0
Rework 7
Under Deviation 0
Containment Action
100 % sorting done at M/s Sangkaj steel end
 
3. Process Flow
Process Flow Description
RM store - RM inspection - Traub - CNC 1st - CNC 2nd - Thread rolling -plating - Final inspection -Dispatch.
 
4. Process Details
Process / Operation Tapping Operation
Outsource No
Machine / Cell Tapping machine
Machine / Cell No. Tapping machine
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MachineCoolant Flow is not ProperLess Coolant flow on TapX
 
6. Inspection Method Analysis (Current)
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size 05 Nos
7. Root Cause Analysis (Occurance)
Why 1 Thread Plug Gauge not Qualify in threading M10X1.25-6H
Why 2 Small Burr stuck in Threading & settled at the bottom thread after Plating.
Why 3 During tapping Small burr not get removed
Why 4 Less Coolant Flow on tap.
Why 5
Root Cause (Occurance) Less Coolant Flow
 
Root Cause Analysis (Outflow)
Why 1 Thread Plug Gauge not Qualify in threading M10X1.25-6H
Why 2 Defective parts get Skipped from Inspection
Why 3 parts Checkied on Sampling Basis.
Why 4 Inadequate Inspection Method
Why 5
Root Cause (Outflow) Inspection Method inadequate
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceCoolant Flow Increased during Tapping. Also Operator given training about not to do tapping if Coolant Flow is not Proper.Mr. Pathan K.H.22/01/202422/01/2024Completed
OutflowInspection done on Sampling Basis, But the Sample Size Increased. Previously only 05 Nos were Checked for thread during Final Inspection, now Sample Size increased to 30%.Mr Mukta23/01/202423/01/2024Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details Inspection done on Sampling Basis, But the Sample Size Increased. Previously only 05 Nos were Checked for thread during Final Inspection, now Sample Size increased to 30%.
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size 30%
10. Evidance of Countermeasure
Occurance (Before) coolant direction is wrong.
630_Occurance_Before.pdf
Occurance (After) Correct the coolant direction & coolant is on tap.
630_Occurance_After.pdf
Outflow (Before) Inadequate Inspection Method
630_Outflow_Before.pdf
Outflow (After) Inspection done on Sampling Basis, But the Sample Size Increased. Previously only 05 Nos were Checked for thread during Final Inspection, now Sample Size increased to 30%.
630_Outflow_After.pdf
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant Applicable for all fork bolt.
 
12. Document Review
Documents ControlPlan, PFMEA, InspCheckSheet
Specify Other Document N/A
 
13. Effectiveness Of Action
Reviewed Quantity 184
Reason for submission Verified and found ok