QFR No - 8000859440
Defect Details
NC No. 8000859440
NC Date 18/01/2024
NC Submission Date
Part No. 520DW01303
Part Name FLANGE BOLT SUZUKI
Supplier Name & Code 100073-SINGLA FORGING (P) LTD
ETL Plant 1117-ETL K-228/9 Suspension
Defect Details NOT AS PER SPECIFICATION-THREAD NG/ OVERSIZE
 
1. Problem Description
Defect Description Fitment issue - Thread NG
Detection Stage Inprocess
Problem Severity Fitment
NG Quantity 28
Is Defect Repeatative? No
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID quality@singlaforging.in
Plant Head/CEO Email ID quality@singlaforging.in
MD Email ID jain@singlaforging.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
5028
0
0
0
0
5028
Check Qty
5028
0
0
0
0
5028
NG Qty
28
0
0
0
0
28
 
Scrap 28
Rework 0
Under Deviation 0
Containment Action
segrsdmklxfd
 
3. Process Flow
Process Flow Description
10 RM 20 FORGING 30 FACING & COLLAR MACHINING 40 ROLLING 50 H/T 60 SURFACE PLATING 70 FINAL INSPECTION 80 PACKING 90 DISPATCH
 
4. Process Details
Process / Operation COLLAR MACHINING
Outsource No
Machine / Cell TURNING TRAUB MACHINING
Machine / Cell No. 01
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MethodTOOL FREQENCY RESHARPNING WAS NOT EFFECTIVETOOL LIFE RECVALIDATION DONEX
ManOPERATOR WAS SKILLEDSKILL MATRIX VERIFIEDX
 
6. Inspection Method Analysis (Current)
Inspection Method Other
Other Inspection Method VISUAL INSPECTION
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
7. Root Cause Analysis (Occurance)
Why 1 THE PROBLEM OCCURED AT FACING & COLLAR MACHINING STAGE OF MANUFATURING SEQUENCE
Why 2 THE FACING TOOL WAS WEAR RESULTED INTO BURR ON FACE
Why 3 THE RESHARPNING FREQUENCY FOR THE CUTTING TOOL WAS DEFINED 200 NO`S
Why 4 RESHARPNINING FREQWUENCY WAS NOT EFFECTIVE, NEED TO BE REVALIDATED AS RAISED CUSTOMER COMPLAINT
Why 5
Root Cause (Occurance) RESHARPNINING FREQWUENCY WAS NOT EFFECTIVE, NEED TO BE REVALIDATED AS RAISED CUSTOMER COMPLAINT
 
Root Cause Analysis (Outflow)
Why 1 VISUALLY INSPECTION WAS NOT EFFECTIVE
Why 2 THOUGH INSPECTOR WAS SKILLED YET IF A FEW PARTS SKIPPED FROM VISUAL INSPECTION
Why 3
Why 4
Why 5
Root Cause (Outflow) THOUGH INSPECTOR WAS SKILLED YET IF A FEW PARTS SKIPPED FROM VISUAL INSPECTION
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceTHOUGH INSPECTOR WAS SKILLED YET IF A FEW PARTS SKIPPED FROM VISUAL INSPECTIONMr. RAM HARESH01/02/202412/02/2024Completed
OutflowDEDICATED PERSON APPOINTEDMr. AMBHORE08/02/202414/02/2024Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System No
Change Details DEDICATED INSPECTOR DEPLOYED, SKILL MATRIX REVIEWED AFTER SHIFT OVER
Inspection Method Other
Other Inspection Method 100% VISUAL
Check Point at Final Inspection No
Checking Freq. 100%
Sampling No
Sample Size 100%
10. Evidance of Countermeasure
Occurance (Before) EVIDANCE ATTACHED
637_Occurance_Before.xlsx
Occurance (After) EVIDANCE ATTACHED
637_Occurance_After.xlsx
Outflow (Before) EVIDANCE ATTACHED
637_Outflow_Before.jpeg
Outflow (After) EVIDANCE ATTACHED
637_Outflow_After.jpeg
 
11. Horizontal Deployment
Horizontal Deployment Required No
Applicable Machine / Model / Plant NO
 
12. Document Review
Documents
Specify Other Document OJT
 
13. Effectiveness Of Action
Reviewed Quantity 352
Reason for submission Checked found ok