QFR No - 8000859440
Defect Details
NC No. | 8000859440 |
NC Date | 18/01/2024 |
NC Submission Date | |
Part No. | 520DW01303 |
Part Name | FLANGE BOLT SUZUKI |
Supplier Name & Code | 100073-SINGLA FORGING (P) LTD |
ETL Plant | 1117-ETL K-228/9 Suspension |
Defect Details | NOT AS PER SPECIFICATION-THREAD NG/ OVERSIZE |
1. Problem Description
Defect Description | Fitment issue - Thread NG |
Detection Stage | Inprocess |
Problem Severity | Fitment |
NG Quantity | 28 |
Is Defect Repeatative? | No |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | quality@singlaforging.in |
Plant Head/CEO Email ID | quality@singlaforging.in |
MD Email ID | jain@singlaforging.com |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
5028
|
0
|
0
|
0
|
0
|
5028
|
Check Qty |
5028
|
0
|
0
|
0
|
0
|
5028
|
NG Qty |
28
|
0
|
0
|
0
|
0
|
28
|
Scrap | 28 |
Rework | 0 |
Under Deviation | 0 |
Containment Action |
---|
segrsdmklxfd |
3. Process Flow
Process Flow Description |
---|
10 RM 20 FORGING 30 FACING & COLLAR MACHINING 40 ROLLING 50 H/T 60 SURFACE PLATING 70 FINAL INSPECTION 80 PACKING 90 DISPATCH |
4. Process Details
Process / Operation | COLLAR MACHINING |
Outsource | No |
Machine / Cell | TURNING TRAUB MACHINING |
Machine / Cell No. | 01 |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Method | TOOL FREQENCY RESHARPNING WAS NOT EFFECTIVE | TOOL LIFE RECVALIDATION DONE | X |
Man | OPERATOR WAS SKILLED | SKILL MATRIX VERIFIED | X |
6. Inspection Method Analysis (Current)
Inspection Method | Other |
Other Inspection Method | VISUAL INSPECTION |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100% |
7. Root Cause Analysis (Occurance)
Why 1 | THE PROBLEM OCCURED AT FACING & COLLAR MACHINING STAGE OF MANUFATURING SEQUENCE |
Why 2 | THE FACING TOOL WAS WEAR RESULTED INTO BURR ON FACE |
Why 3 | THE RESHARPNING FREQUENCY FOR THE CUTTING TOOL WAS DEFINED 200 NO`S |
Why 4 | RESHARPNINING FREQWUENCY WAS NOT EFFECTIVE, NEED TO BE REVALIDATED AS RAISED CUSTOMER COMPLAINT |
Why 5 | |
Root Cause (Occurance) | RESHARPNINING FREQWUENCY WAS NOT EFFECTIVE, NEED TO BE REVALIDATED AS RAISED CUSTOMER COMPLAINT |
Root Cause Analysis (Outflow)
Why 1 | VISUALLY INSPECTION WAS NOT EFFECTIVE |
Why 2 | THOUGH INSPECTOR WAS SKILLED YET IF A FEW PARTS SKIPPED FROM VISUAL INSPECTION |
Why 3 | |
Why 4 | |
Why 5 | |
Root Cause (Outflow) | THOUGH INSPECTOR WAS SKILLED YET IF A FEW PARTS SKIPPED FROM VISUAL INSPECTION |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Occurance | THOUGH INSPECTOR WAS SKILLED YET IF A FEW PARTS SKIPPED FROM VISUAL INSPECTION | Mr. RAM HARESH | 01/02/2024 | 12/02/2024 | Completed |
Outflow | DEDICATED PERSON APPOINTED | Mr. AMBHORE | 08/02/2024 | 14/02/2024 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | No |
Change Details | DEDICATED INSPECTOR DEPLOYED, SKILL MATRIX REVIEWED AFTER SHIFT OVER |
Inspection Method | Other |
Other Inspection Method | 100% VISUAL |
Check Point at Final Inspection | No |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100% |
10. Evidance of Countermeasure
Occurance (Before) |
EVIDANCE ATTACHED 637_Occurance_Before.xlsx |
Occurance (After) |
EVIDANCE ATTACHED 637_Occurance_After.xlsx |
Outflow (Before) |
EVIDANCE ATTACHED 637_Outflow_Before.jpeg |
Outflow (After) |
EVIDANCE ATTACHED 637_Outflow_After.jpeg |
11. Horizontal Deployment
Horizontal Deployment Required | No |
Applicable Machine / Model / Plant | NO |
12. Document Review
Documents | |
Specify Other Document | OJT |
13. Effectiveness Of Action
Reviewed Quantity | 352 |
Reason for submission | Checked found ok |