QFR No - 8000859453
Defect Details
NC No. 8000859453
NC Date 18/01/2024
NC Submission Date
Part No. F2LG03702B
Part Name SEAT PIPE (K1 UG)
Supplier Name & Code 100648-JOTIBA TECHNOLOGIES PVT.LTD.
ETL Plant 1117-ETL K-228/9 Suspension
Defect Details NOT AS PER SPECIFICATION-OPERATION MISSING
 
1. Problem Description
Defect Description Compression and DF hole missing
Detection Stage Inprocess
Problem Severity Function
NG Quantity 1
Is Defect Repeatative? No
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID accjotiba@gmail.com
Plant Head/CEO Email ID sanghavi.rajesh@sanghavigroup.co.in
MD Email ID jotibatech@gmail.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
1000
0
0
1500
2500
5000
Check Qty
1000
0
0
1500
2500
5000
NG Qty
1
0
0
0
0
1
 
Scrap 0
Rework 1
Under Deviation 0
Containment Action
Add special gauge for inspection of D.F Hole and Compression Hole at final inspection.
 
3. Process Flow
Process Flow Description
10. RM Inspection,20.Parting off,30.Chmafering,40.Weighing,50.Draw forging,60.Hex Forging,70.Rough Grinding, 80.Collar Machining,90.Total length facing and boring, 100 Piercing, 110.DF hole Chamfer, 120.Compression hole Chamfer, 130.ID Reaming, 140.Tapping, 150.Finish Grinding, 160.Final Inspection, 170.ID brush Cleaning, 180.Ultrasonic Cleaning, 190.Apply antirust oil, 200.Packing and dispatch.
 
4. Process Details
Process / Operation 100. Piercing.
Outsource No
Machine / Cell Mechanical Press
Machine / Cell No. PM-01
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MethodInspect part at final inspection visually.okO
 
6. Inspection Method Analysis (Current)
Inspection Method Sp. Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size Sampling
7. Root Cause Analysis (Occurance)
Why 1 D.F Hole and Compression hole missing part produces.
Why 2 While set-up during stroke adjustment some parts produced of half punch & No punch
Why 3 Operator Not able to setup and produced first piece OK. (In setup by operator half punch and no punch parts produce).
Why 4
Why 5
Root Cause (Occurance) Need to change responsibility of setup change from operator to supervisor.
 
Root Cause Analysis (Outflow)
Why 1 D.F Hole and Compression Hole missing not detected at outflow.
Why 2 Inspect part at outflow is visually
Why 3 No special gauge for inspection.
Why 4
Why 5
Root Cause (Outflow) No special gauge for inspection of D.F Hole and Compression Hole inspection.
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OutflowAdd special gauge for inspection of compression hole 100% and D.F hole sampling.Gore23/01/202418/01/2024Completed
OccuranceChange Responsibility of die setup loading and unloading operator to supervisor.Mr. Gaurav23/01/202418/01/2024Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details By using special gauge.
Inspection Method Sp. Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size Chart
10. Evidance of Countermeasure
Occurance (Before) Due operator setup of piercing and machine.
640_Occurance_Before.xlsx
Occurance (After) Responsibility of supervisor setup die and machine.
640_Occurance_After.xlsx
Outflow (Before) Inspect part as per sampling plan and visually.
640_Outflow_Before.xlsx
Outflow (After) Using special gauge for inspection.
640_Outflow_After.xlsx
 
11. Horizontal Deployment
Horizontal Deployment Required No
Applicable Machine / Model / Plant NA
 
12. Document Review
Documents
Specify Other Document Special Gauge
 
13. Effectiveness Of Action
Reviewed Quantity 251
Reason for submission Verified and found ok