QFR No - 8000859513
Defect Details
NC No. | 8000859513 |
NC Date | 19/01/2024 |
NC Submission Date | |
Part No. | F1LG00902B |
Part Name | SEAT PIPE -K86A |
Supplier Name & Code | 100538-NARINDER PARKASH AND CO |
ETL Plant | 1146-ETL Suspension Narasapura |
Defect Details | MIX UP OTHER MODEL-NOT USING K0PG MODEL MIX UP AT NP SUP |
1. Problem Description
Defect Description | K86 seat pipe wrong part supplied to ETL not using KOPG FF model MIX up at supplier end . |
Detection Stage | Receipt |
Problem Severity | Fitment |
NG Quantity | 250 |
Is Defect Repeatative? | Yes |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | quality@npcindustries.in |
Plant Head/CEO Email ID | anand@npcindustries.in |
MD Email ID | ajay@npcindustries.in |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
4400
|
0
|
0
|
400
|
0
|
4800
|
Check Qty |
4400
|
0
|
0
|
400
|
0
|
4800
|
NG Qty |
250
|
0
|
0
|
0
|
0
|
250
|
Scrap | 0 |
Rework | 250 |
Under Deviation | 0 |
Containment Action |
---|
segregated all material at both end |
3. Process Flow
Process Flow Description |
---|
Cutting - Draw - Forging - Rough Grinding - Punching - CNC Head Turning - CNC Tail Facing - Tapping & Chamfering - Final Grinding - Final Inspection - Cleaning - RPO Oiling - Packing & Dispatch. |
4. Process Details
Process / Operation | Packing station |
Outsource | No |
Machine / Cell | STATION-2 |
Machine / Cell No. | NA |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Man | Quality Inspector Negligence | Verified and found OK. No linkage with defect | O |
Tool | Wrong gauge and instrument use | Measuring instrument is found calibrated & ok condition. | O |
Method | material stock place not define | Material stock place was identified | O |
Method | Packing Method Inadequate | Inside material polybag was not identified | X |
Method | Holding the part not as per define method | Verified and found OK. No linkage with defect | O |
Method | Wrong identification tag | After verification we found wrong identification tag found | X |
6. Inspection Method Analysis (Current)
Inspection Method | Gauge |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100% |
7. Root Cause Analysis (Occurance)
Why 1 | Other model box replace with K-86 box |
Why 2 | mixing was occur in Packing station |
Why 3 | Other model parts box put together with the box of k-86 model |
Why 4 | Identification mark was not available before final packing |
Why 5 | |
Root Cause (Occurance) | Identification mark was not available before final packing |
Root Cause Analysis (Outflow)
Why 1 | Other model box replace with K-86 box |
Why 2 | Material was mixed after final inspection |
Why 3 | wrong sticker pasted as per identification mark at dispatch station. |
Why 4 | Verification point was not available at dispatch station |
Why 5 | |
Root Cause (Outflow) | Verification point was not available at dispatch station |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Occurance | Model details should be written at the starting of packing | Mr. Ankush | 22/01/2024 | 22/01/2024 | Completed |
Occurance | Q-alert to be displayed at final and packing station | Mr. Princ | 20/01/2024 | 20/01/2024 | Completed |
Outflow | Sample inspection started of packed lots after packing. | . Mr. Ankush | 22/01/2024 | 22/01/2024 | Completed |
Outflow | Q-alert to be displayed at Dispatch station | Mr. Princ | 20/01/2024 | 20/01/2024 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | Yes |
Change Details | Sampling method to be used for reverification. |
Inspection Method | Other |
Other Inspection Method | Visual |
Check Point at Final Inspection | No |
Checking Freq. | Sampling |
Sampling | No |
Sample Size | 5 box/lot |
10. Evidance of Countermeasure
Occurance (Before) |
Model details was written at the end of packing. 645_Occurance_Before.jpg |
Occurance (After) |
Model details should be written at the starting of packing. 645_Occurance_After.jpg |
Outflow (Before) |
No verification done 645_Outflow_Before.jpg |
Outflow (After) |
Sample inspection started of packed lots after packing. 645_Outflow_After.jpg |
11. Horizontal Deployment
Horizontal Deployment Required | Yes |
Applicable Machine / Model / Plant | All similar models . |
12. Document Review
Documents | ControlPlan, PFMEA, WISOP |
Specify Other Document | No |
13. Effectiveness Of Action
Reviewed Quantity | 10000 |
Reason for submission | Reviewed next 3 lots no mixes up found ok |