QFR No - 8000861163
Defect Details
NC No. | 8000861163 |
NC Date | 30/01/2024 |
NC Submission Date | |
Part No. | 550LZ00102 |
Part Name | SPACER L 50-PRF001 |
Supplier Name & Code | 100990-JAIRAJ ANCILLARIES PVT LTD |
ETL Plant | 1118-ETL E-92,93 Suspension |
Defect Details | DIAMETER OVER SIZE-OVALITY & 33±0.1 GRUE OD OVER SIZE |
1. Problem Description
Defect Description | Groove OD over size |
Detection Stage | Inprocess |
Problem Severity | Fitment |
NG Quantity | 114 |
Is Defect Repeatative? | No |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | planthead.aurangabad@jairajgroup.com |
Plant Head/CEO Email ID | vp@jairajgroup.com |
MD Email ID | rajiv@jairajgroup.com |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
1400
|
0
|
0
|
0
|
0
|
1400
|
Check Qty |
1400
|
0
|
0
|
0
|
0
|
1400
|
NG Qty |
114
|
0
|
0
|
0
|
0
|
114
|
Scrap | 114 |
Rework | 0 |
Under Deviation | 0 |
Containment Action |
---|
Immediately visited customer end for problem identification & 100% checking of all available stock at customer end completed |
3. Process Flow
Process Flow Description |
---|
Receipt of raw material, Inward inspection , storage, Material issue, Injection molding, Machining, Deflashing & final inspection, Packing & labelling, Pre dispatch inspection, despatch |
4. Process Details
Process / Operation | Injection Molding |
Outsource | No |
Machine / Cell | Injection molding machine |
Machine / Cell No. | IM-5 |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Method | Sampling Inspection at Final Inspection stage & on machine | Verified that at FI inspection by gauge on sampling basis & operator was checking after every hour | X |
Method | Part clamping not correct | Verified that part clamping on machine was not correct | X |
Man | Operator having less awareness | Varified & found that operator was having less awareness about the issue | X |
Tool | Tool not ok / wear out | Verified that there was no problem in tool | O |
Material | Use of improper material | Veried that material used was as per specifications | O |
Machine | Improper Cooling time in Injection moulding | Verified and found that cooling time was as per specified | O |
Machine | Jaw wear out in machining | Verified and found that jaw condition was ok | O |
Method | Process parameters not followed | Verified that process parameters were as specified | O |
6. Inspection Method Analysis (Current)
Inspection Method | Gauge |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | Sampling |
Sampling | No |
Sample Size | Aslot size |
7. Root Cause Analysis (Occurance)
Why 1 | Groove OD O/S - Req Specification 33.95+/- 0.1 mm & found oval |
Why 2 | While machining for groove equal material not removed from part OD |
Why 3 | Due to part clamping was not centered in jaws |
Why 4 | Flashes not removed from part before clamping |
Why 5 | Manual error |
Root Cause (Occurance) | Flashes on part were not removed by the operator prior its loading for machining ( Manual error) |
Root Cause Analysis (Outflow)
Why 1 | Groove OD O/S - Req Specification 33.95+/- 0.1 mm & found oval |
Why 2 | Part skipped from machine & Final inspection stage |
Why 3 | Inspection on sampling basis on machine by operator & by inspector at FI |
Why 4 | |
Why 5 | |
Root Cause (Outflow) | Inspection on sampling basis on machine by operator & by inspector at FI |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Occurance | Training provided to operator on removing flashes from part , prior to loading on machine | Production | 24/02/2024 | 24/02/2024 | Completed |
Outflow | 1. Parts are checking 100% with GO Gauge for groove OD at FI with Identification mark. 2. Now 100% parts are checked by gauge (groove OD 33.95 +/-0.1 mm) by operator on machine. 3. Displayed OK/NG samples at work station & also displayed OPL. | QA HOD | 24/02/2024 | 24/02/2024 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | Yes |
Change Details | 1. Parts are checking 100% with GO Gauge for groove OD at FI by inspector with Identification mark. 2. Now 100% parts are checked by gauge (groove OD 33.95 +/-0.1 mm) by operator on machine |
Inspection Method | Gauge |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100% |
10. Evidance of Countermeasure
Occurance (Before) |
Operator having less awareness about the issue 656_Occurance_Before.xlsx |
Occurance (After) |
Training provided to the operator ( Training Record) 656_Occurance_After.pdf |
Outflow (Before) |
Inspection on Sampling basis with gauge on machine by operator & at Final inspection by inspector 656_Outflow_Before.xlsx |
Outflow (After) |
100% Inspection with gauge by operator on machine & by inspector at FI 656_Outflow_After.xlsx |
11. Horizontal Deployment
Horizontal Deployment Required | No |
Applicable Machine / Model / Plant | Not Applicable |
12. Document Review
Documents | |
Specify Other Document | NO |
13. Effectiveness Of Action
Reviewed Quantity | 11000 |
Reason for submission | after action implementation no any parts found defective. |