QFR No - 8000862067
Defect Details
NC No. 8000862067
NC Date 07/02/2024
NC Submission Date
Part No. 520DZ01712
Part Name FORK BOLT DF181085
Supplier Name & Code 100189-SANGKAJ STEEL PVT LTD.
ETL Plant 1117-ETL K-228/9 Suspension
Defect Details NOT AS PER SPECIFICATION-M26 THREAD FITMENT ISSUE
 
1. Problem Description
Defect Description M26 thread fitment NG
Detection Stage Inprocess
Problem Severity Fitment
NG Quantity 150
Is Defect Repeatative? Yes
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID qualityassurance@sangkaj.com
Plant Head/CEO Email ID qualityassurance@sangkaj.com
MD Email ID anirudh.2007@hotmail.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
250
0
0
200
0
450
Check Qty
250
0
0
200
0
450
NG Qty
150
0
0
200
0
350
 
Scrap 0
Rework 150
Under Deviation 0
Containment Action
100 % sorting at ETL end with special identification. Also 100% sorting done at M/s Sangkaj Steel End with special identification.
 
3. Process Flow
Process Flow Description
RM Store - RM Inspection - Traub - Pre roll dia Grinding -Tapping M10 - Thread Rolling M26 - Plating - Final inspection - Dispatch.
 
4. Process Details
Process / Operation Thread Rolling
Outsource No
Machine / Cell Thread Rolling
Machine / Cell No. Rolling - 02
5. Problem Analysis
Type Possible Cause Fact Verification Jud
ToolWrong tool used for operation.Wrong tool used for operation.O
MachineMachine parameter not okay at Grinding stage .Parameter observed at operation stage & found okay.O
MachineMachine parameter not okay at machining stage.Parameter observed at operation stage & found okay.O
Methodinspection method not okayLess sampling frequency.X
ManSkipped from inspection.NG part found at customer end.X
MaterialWrong material used.Verified the TC report & Found okay.O
MachineMachine parameter not okay at machining stage .Parameter observed at operation stage & found okay.O
MachinePart dimn not as per drawingPre roll dimn observed at higher side.X
MethodLoading & Unloading method not okay.During Gemba visit at operation stage loading & unloading method observed okay.O
 
6. Inspection Method Analysis (Current)
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size 05 Nos
7. Root Cause Analysis (Occurance)
Why 1 M26 Threading not okay.
Why 2 After plating threading not qualified in mating part.
Why 3 On part minor dia found at higher side.
Why 4 On part Pre roll dia observed at higher side
Why 5 Operator is not aware about effect of parts makes at higher side of specification.
Root Cause (Occurance) Operator is not aware about effect of parts makes at higher side of specification.
 
Root Cause Analysis (Outflow)
Why 1 M26 Threading not okay.
Why 2 Skipped from Inspection
Why 3 defect not detect in during final inspection.
Why 4 Less sampling frequency.
Why 5
Root Cause (Outflow) Less sampling frequency.
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccurancePre roll diameter to be maintain at lower side of specification.Mr Raut.23/01/202423/01/2024Completed
OutflowSampling inspection frequency increase at final inspection from 05 nos to 50 nos.Mrs Mukta23/01/202423/01/2024Completed
OccuranceTraining & Awareness given to operator.Mr Anil22/01/202422/01/2024Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System No
Change Details N/A
Inspection Method Other
Other Inspection Method Mating part
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size 50 Nos
10. Evidance of Countermeasure
Occurance (Before) Operator is not aware about effect of parts makes at higher side of specification.
661_Occurance_Before.pdf
Occurance (After) Pre roll diameter to be maintain at lower side of specification.
661_Occurance_After.pdf
Outflow (Before) Less inspection sampling frequency on mating part.
661_Outflow_Before.pdf
Outflow (After) Sampling inspection frequency increase at final inspection from 05 nos to 50 nos
661_Outflow_After.pdf
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant Applicable for all type of fork bolt
 
12. Document Review
Documents ControlPlan, PFMEA, InspCheckSheet
Specify Other Document N/A
 
13. Effectiveness Of Action
Reviewed Quantity 596
Reason for submission Verified and found ok