QFR No - 8000862162
Defect Details
NC No. | 8000862162 |
NC Date | 07/02/2024 |
NC Submission Date | |
Part No. | F2KH01002B |
Part Name | REBOUND SPRING-XF121 |
Supplier Name & Code | 101159-TECHNOMAT SPRINGS |
ETL Plant | 1117-ETL K-228/9 Suspension |
Defect Details | NOT AS PER SPECIFICATION-MIX-UP |
1. Problem Description
Defect Description | Other model part mix-up |
Detection Stage | Inprocess |
Problem Severity | Function |
NG Quantity | 100 |
Is Defect Repeatative? | No |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | quality@technomatsprings.com |
Plant Head/CEO Email ID | technomatsprings@gmail.com |
MD Email ID | patilsadanand@technomatsprings.com |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
3000
|
0
|
0
|
1800
|
0
|
4800
|
Check Qty |
3000
|
0
|
0
|
1800
|
0
|
4800
|
NG Qty |
100
|
0
|
0
|
0
|
0
|
100
|
Scrap | 0 |
Rework | 100 |
Under Deviation | 0 |
Containment Action |
---|
Checked all material at customer end and pipeline material also. |
3. Process Flow
Process Flow Description |
---|
R/m In-warding Inspection > Coiling > Stress Relieving-1 > Grinding > Shot Peening > Stress Relieving-2 > Final Inspection > Oiling > Packing > Dispatch. |
4. Process Details
Process / Operation | Coiling |
Outsource | No |
Machine / Cell | - |
Machine / Cell No. | - |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Material | Wrong Material / Grade | Supplier RMTC Report checked found Ok | O |
Machine | - | - | O |
Tool | Tool Wear Out | Tool Monitoring Card Verified found ok | O |
Man | Unskilled Operator | Skilled matrix found ok | O |
Method | Without looking the complete part no. | Dispatched wrong material without verify complete part no. | X |
6. Inspection Method Analysis (Current)
Inspection Method | Other |
Other Inspection Method | Visual |
Check Point at Final Inspection | Yes |
Checking Freq. | Sampling |
Sampling | No |
Sample Size | 30 Nos |
7. Root Cause Analysis (Occurance)
Why 1 | Material Mix-up at customer end |
Why 2 | Due to wrong material dispatched |
Why 3 | the material was not identified due to the similar part kept aside of the each other, and packing std was same. |
Why 4 | |
Why 5 | |
Root Cause (Occurance) | the material was not identified due to the similar part kept aside of the each other, and packing was same. |
Root Cause Analysis (Outflow)
Why 1 | Material Mix-up at customer end |
Why 2 | Due to wrong material dispatched |
Why 3 | Separate place defined for the similar parts and packing (Polybag) change for to avoid the mix-up issues. |
Why 4 | |
Why 5 | |
Root Cause (Outflow) | Separate place defined for the similar parts and packing (Polybag) change for to avoid the mix-up issues. |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Outflow | 1) Location defined for the similar springs 2) Training given to related person. | Mr. Anuj Shelke | 29/02/2024 | 29/02/2024 | Completed |
Occurance | Polybag color change to avoid mix-up issues. | Mr. Anuj Shelke | 29/02/2024 | 29/02/2024 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | No |
Change Details | NA |
Inspection Method | Other |
Other Inspection Method | Visual |
Check Point at Final Inspection | Yes |
Checking Freq. | Sampling |
Sampling | No |
Sample Size | 30 Nos |
10. Evidance of Countermeasure
Occurance (Before) |
Packing Before 658_Occurance_Before.pdf |
Occurance (After) |
Packing After 658_Occurance_After.pdf |
Outflow (Before) |
Outflow Before 658_Outflow_Before.pdf |
Outflow (After) |
Outflow After 658_Outflow_After.pdf |
11. Horizontal Deployment
Horizontal Deployment Required | Yes |
Applicable Machine / Model / Plant | For the similar type of products. |
12. Document Review
Documents | PackingStd |
Specify Other Document | NA |
13. Effectiveness Of Action
Reviewed Quantity | 438 |
Reason for submission | Found ok |