QFR No - 8000862164
Defect Details
NC No. | 8000862164 |
NC Date | 07/02/2024 |
NC Submission Date | |
Part No. | 520DZ00212 |
Part Name | FORK BOLT K60-(DS181012) |
Supplier Name & Code | 101263-SINGLA PRECISION SCREWS |
ETL Plant | 1117-ETL K-228/9 Suspension |
Defect Details | NOT AS PER SPECIFICATION-M10 THREAD GO NOT QUALIFYING & NOGO QUAL |
1. Problem Description
Defect Description | M10 THREAD GO NOT QUALIFYING & NOGO QUALIFYING |
Detection Stage | Receipt |
Problem Severity | Fitment |
NG Quantity | 10 |
Is Defect Repeatative? | Yes |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | quality@singlaprecision.com |
Plant Head/CEO Email ID | quality@singlaprecision.com |
MD Email ID | aditya@singlaprecision.com |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
800
|
0
|
0
|
0
|
0
|
800
|
Check Qty |
800
|
0
|
0
|
0
|
0
|
800
|
NG Qty |
28
|
0
|
0
|
0
|
0
|
28
|
Scrap | 28 |
Rework | 0 |
Under Deviation | 0 |
Containment Action |
---|
Stock Check 100% at our end |
3. Process Flow
Process Flow Description |
---|
Forging ,CNC-IST, CNC-2ND, BUFFING ,ROLLING ,SURFACE ,TREATMENT, FINAL INSPECTION -PACKING |
4. Process Details
Process / Operation | CNC IST |
Outsource | No |
Machine / Cell | 01 |
Machine / Cell No. | 02 |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Material | RM GRADE AND SIZE NOT OK | VALIDATED AND FOUND OK | O |
Method | INSPECTION METHOD NOT EFFECTIVE | INSPECTION DONE AS PER SAMPLING PLAN SO PART SKIPPED FROM INSPECTION | X |
Tool | TOOL WEAROUT | VALIDATED AND FOUND OK | O |
Man | UNWAWARENESS OF OPERATOR | VALIDATED AND FOUND OPERATOR WAS LOW LEVEL | X |
Machine | WORNG OFFSET | OFFSET NOT INTERLOCK | X |
6. Inspection Method Analysis (Current)
Inspection Method | Instrument |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | Sampling |
Sampling | No |
Sample Size | 50 |
7. Root Cause Analysis (Occurance)
Why 1 | M10 thread fitment NG (not qualifying to minor diameter pin 8.647, qualifying minor diameter pin 8.912 -) |
Why 2 | Part minor dia over size because operator wrong offset give to machine |
Why 3 | because offset not interlock |
Why 4 | CNC Machine Programming did not set how much offset the operator could give only for |
Why 5 | Machine checking Manor dia PPG gauge not 100% checked |
Root Cause (Occurance) | Part minor dia over size because operator wrong offset give to machine |
Root Cause Analysis (Outflow)
Why 1 | M10 thread fitment NG (not qualifying to minor diameter pin 8.647, qualifying minor diameter pin 8.912 -) |
Why 2 | The Problem occurred at checking method |
Why 3 | Final inspection only part checked as per sampling plan |
Why 4 | operator part 100% not checked for ppg |
Why 5 | |
Root Cause (Outflow) | INSPECTION DONE AS PER SAMPLING PLAN SO PART SKIPPED FROM INSPECTION |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Occurance | MACHINE OFFSET INTERLOCK | ANIL | 09/03/2024 | 09/03/2024 | Completed |
Outflow | CHECKING FREQ CHANGE 100 % CHECKING FINAL INSPECTION UPDATE | GANESH MAURYA | 09/03/2024 | 09/03/2024 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | Yes |
Change Details | Inspection frequency change to 100% |
Inspection Method | Gauge |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | no |
10. Evidance of Countermeasure
Occurance (Before) |
OFFSET NOT INTERLOCK 663_Occurance_Before.xlsx |
Occurance (After) |
OFFSET INTERLOCK 663_Occurance_After.png |
Outflow (Before) |
CHECKING FREQ NOT CHANGE AS PER SAMPLING PLAN 663_Outflow_Before.png |
Outflow (After) |
CHECKING FREQ CHANGE 100 % CHECKING FINAL INSPECTION UPDATE 663_Outflow_After.png |
11. Horizontal Deployment
Horizontal Deployment Required | No |
Applicable Machine / Model / Plant | CNC MACHINE |
12. Document Review
Documents | ControlPlan, PokayokeCheckSheet, InspCheckSheet |
Specify Other Document | POKA YOKA & CP |
13. Effectiveness Of Action
Reviewed Quantity | 150 |
Reason for submission | 8. Countermeasure ( Occurrence , Outflow & System side Actions ) - NOT UPDATED |