QFR No - 8000862167
Defect Details
NC No. | 8000862167 |
NC Date | 07/02/2024 |
NC Submission Date | |
Part No. | F2LG05902B |
Part Name | SEAT PIPE (K17B/D) |
Supplier Name & Code | 100539-N P ENTERPRISES |
ETL Plant | 1117-ETL K-228/9 Suspension |
Defect Details | NOT AS PER SPECIFICATION-OD OVERSIZE |
1. Problem Description
Defect Description | OD oversize |
Detection Stage | Inprocess |
Problem Severity | Fitment |
NG Quantity | 10 |
Is Defect Repeatative? | No |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | quality@npcindustries.in |
Plant Head/CEO Email ID | anand@npcindustries.in |
MD Email ID | ajay@npcindustries.in |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
1500
|
6000
|
4500
|
0
|
0
|
12000
|
Check Qty |
1500
|
6000
|
4500
|
0
|
0
|
12000
|
NG Qty |
10
|
30
|
0
|
0
|
0
|
40
|
Scrap | 0 |
Rework | 40 |
Under Deviation | 0 |
Containment Action |
---|
Segregated all material at customer and NPC end. |
3. Process Flow
Process Flow Description |
---|
PFD |
4. Process Details
Process / Operation | Finish Grinding |
Outsource | No |
Machine / Cell | Centerless grinding |
Machine / Cell No. | CG-04 |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Method | NG parts skipped at Final Inspection | Verified found not OK | X |
Machine | Control wheel Size NG | Verified and found OK. No linkage with defect | O |
Method | Wrong parameter use | All parameter was followed as per std. | O |
Tool | Wrong Instrument used for measurement | Verified found OK | O |
Machine | Non uniform removal of material after Grinding | During defect verification and simulation it was observed that there is less material removal from t | X |
6. Inspection Method Analysis (Current)
Inspection Method | Gauge |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | Sampling |
Sampling | No |
Sample Size | as per std |
7. Root Cause Analysis (Occurance)
Why 1 | Non uniform removal of material after Grinding |
Why 2 | Non uniform removal of material after Grinding |
Why 3 | Taper in control wheel |
Why 4 | Control Wheel Dressing not done after model change |
Why 5 | |
Root Cause (Occurance) | Control Wheel Dressing not done after model change |
Root Cause Analysis (Outflow)
Why 1 | NG parts skipped at Final Inspection |
Why 2 | NG parts skipped at Final Inspection |
Why 3 | Could not be detected at Final Inspection |
Why 4 | Skipped in Sampling at Final Inspection |
Why 5 | Sampling plan inadequate |
Root Cause (Outflow) | Sampling plan inadequate |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Occurance | Dressing made mandatory for both wheels (Control wheel & Grinding wheel) after model change at Centre less Grinding machine). | Mr. Gurpreet Singh | 10/02/2024 | 08/02/2024 | Completed |
Outflow | Single Sampling plan to be replaced with double sampling plan . | Mr. Ankush | 08/02/2024 | 08/02/2024 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | Yes |
Change Details | Single Sampling plan to be replaced with double sampling plan . |
Inspection Method | Gauge |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | Sampling |
Sampling | No |
Sample Size | as per std |
10. Evidance of Countermeasure
Occurance (Before) |
Control and grinding wheel dressing done as per freezed qty 665_Occurance_Before.png |
Occurance (After) |
Dressing made mandatory for both wheels (Control wheel & Grinding wheel) after model change at Centre less Grinding machine). 665_Occurance_After.png |
Outflow (Before) |
Single Sampling plan used 665_Outflow_Before.jpg |
Outflow (After) |
Single Sampling plan to be replaced with double sampling plan 665_Outflow_After.png |
11. Horizontal Deployment
Horizontal Deployment Required | Yes |
Applicable Machine / Model / Plant | All similar models |
12. Document Review
Documents | ControlPlan, PFMEA, WISOP, InspCheckSheet |
Specify Other Document | No |
13. Effectiveness Of Action
Reviewed Quantity | 517 |
Reason for submission | Found ok |