QFR No - 8000862175
Defect Details
NC No. 8000862175
NC Date 07/02/2024
NC Submission Date
Part No. 520PC03307
Part Name UNDER BKT SUB-ASSY. K3
Supplier Name & Code 100061-BAJAJSONS LIMITED
ETL Plant 1117-ETL K-228/9 Suspension
Defect Details OPERATION MISSING-M16 OPERAION MISSING
 
1. Problem Description
Defect Description OPERATION MISSING-M16 OPERAION MISSING
Detection Stage Customer End
Problem Severity Fitment
NG Quantity 1
Is Defect Repeatative? No
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID pushpendra.singh@bajajsons.com
Plant Head/CEO Email ID crbansal@bajajsons.com
MD Email ID sanjay.bajaj@bajajsons.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
50
800
100
100
200
1250
Check Qty
50
300
0
100
200
650
NG Qty
1
0
0
0
0
1
 
Scrap 0
Rework 1
Under Deviation 0
Containment Action
No material at customer end .Inspection started in warehouse & checked 300 pcs. Out of 800 pcs. and found all material ok ,Rest 500+100pcs(Transit) will be checked before Dispatch to ETL as per their requirement. At our end we checked our F.G Stock and WIP material (Qty. 100+200) and found ok.
 
3. Process Flow
Process Flow Description
PRESS FITTING, MIG WELDING ,COUNTER SIDE BORES(TOP) , COUNTER SIDE BORES(BOTTOM SIDE) ,SLITTING(LEFT SIDE) , SLITTING(RIGHT SIDE) BROACHING(CHAMFER AT SLITTING )(LEFT AND RIGHT SIDE) , COUNTERING AT HOLE DIA.10.50(LEFT & RIGHT) , COUNTERING AT HOLE DIA. 8.60(LEFT & RIGHT) , DEBURRING AT MACHINE AREA , CARBON CLEANING-BORE OPENING , 2-TAPPING M6X1-6H , TAPPING M10 X 1.5 -6H(LEFT SIDE) , TAPPING M10 X 1.5 -6H(RIGHT SIDE) , 2-TAPPING 2-M6 X 1-6H , BUSH TAPPING M16 X 1.5-6H , STRAIGHTENING (PARALLISM INSPECTION) , DIE PASS OUT TO REMOVE THE DENT AND PHASPHATING SLIDGE (M30X1P-6H) , FINAL INSPECTION , PRE- DISPATCH INSPECTION PACKING &DISPATCH.
 
4. Process Details
Process / Operation BUSH TAPPING M16X 1.5-6H
Outsource No
Machine / Cell TMS
Machine / Cell No. 03
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MachineMachine not working during tapping processDuring verification found that machine is ok (No breakdown)O
MethodMultiple part taking from trolley for tapping & kept at machine tableDuring verification found that operator is taking more then one part during tapping at tableX
ManUnskilled manpowerSkilled manpower deployed at inspectionO
ToolWorn out tap used & due to tapping not performedTap was ok because tap life monitoringO
MethodPart skipped from tapping machine(Moved from previous operation to next operation)During verification found that complete trolley moved to next stageO
MethodImproper handling of NG part during final inspectionDuring verification found that checker was did not mark on NG part during inspectionX
MaterialHardness more in partDuring verification found bush material was okO
 
6. Inspection Method Analysis (Current)
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 5
7. Root Cause Analysis (Occurance)
Why 1 Tapping miss of M16x1.5 part skipped
Why 2 Tapping not performed due to part not loaded at machine
Why 3 Due to mix-up of tapping done & without tapping parts
Why 4 Mix-up due to multi parts taken from trolley & kept of machine table
Why 5 Neglegency of machine operator
Root Cause (Occurance) Mix-up due to multi parts taken from trolley & kept of machine table, resulting NG part mix up & reached at next stage
 
Root Cause Analysis (Outflow)
Why 1 NG part skipped from final inspection & reached at customer end
Why 2 NG part mix-up in ok material
Why 3 Mix-up in ok material due to no marking on NG part
Why 4 No marking on NG part due to negligency of checker
Why 5
Root Cause (Outflow) No marking on NG part due to negligency of checker
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OutflowAwareness given to checkers for NG part handlingIrfan Ahmed16/02/202415/02/2024Completed
OccuranceOPL made & awareness given to machine operators for single part movement from trolley to avoid mix-upJasbir Singh15/02/202415/02/2024Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System No
Change Details N/A
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 5
10. Evidance of Countermeasure
Occurance (Before) Mix-up due to multi parts taken from trolley & kept of machine table
671_Occurance_Before.jpg
Occurance (After) Single part pick up from trolly for Bush Tapping M16X1.5.
671_Occurance_After.jpg
Outflow (Before) No marking on NG part due to negligency of checker
671_Outflow_Before.jpg
Outflow (After) Rework part move after marking as a decided place.
671_Outflow_After.jpg
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant TMS -03/AVENGER & K-17 B/D/BSL U-III.
 
12. Document Review
Documents PFMEA, WISOP
Specify Other Document NO
 
13. Effectiveness Of Action
Reviewed Quantity 255
Reason for submission Checked and found ok