QFR No - 8000862271
Defect Details
NC No. 8000862271
NC Date 07/02/2024
NC Submission Date
Part No. 520HQ00202
Part Name ORIFICE VALVE
Supplier Name & Code 100141-ARVIND AUTOMOTIVE (INDIA) PVT.
ETL Plant 1118-ETL E-92,93 Suspension
Defect Details NOT AS PER SPECIFICATION-WRONG MATERIAL(520HQ00502
 
1. Problem Description
Defect Description NOT AS PER SPECIFICATION-WRONG MATERIAL (520HQ00502)
Detection Stage Receipt
Problem Severity Aesthetic
NG Quantity 20000
Is Defect Repeatative? No
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID automotivearvind@yahoo.com
Plant Head/CEO Email ID automotivearvind@yahoo.com
MD Email ID cheemaarvind@yahoo.in
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
20000
20000
0
25000
10000
75000
Check Qty
20000
20000
0
25000
10000
75000
NG Qty
20000
0
0
0
0
20000
 
Scrap 0
Rework 0
Under Deviation 20000
Containment Action
1-SHORT QTY SEND TO LOGISTICS TO MAINTAINED ACTUAL PART NUMBER AND LOT QTY ALSO 2- LOGISTICS PERSON VERIFY THE MATERIAL AS PER INVOICE NO WHICH IS ALREADY MENTION IN TAGS AND NUMBER OF BOXES ALSO
 
3. Process Flow
Process Flow Description
BLANKING+PUNCHING
 
4. Process Details
Process / Operation PUNCHING
Outsource No
Machine / Cell POWER PRESS
Machine / Cell No. PP 05
5. Problem Analysis
Type Possible Cause Fact Verification Jud
ManUnskilled helperOperator did not aware about Tags and invoiceX
 
6. Inspection Method Analysis (Current)
Inspection Method Other
Other Inspection Method Visual
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
7. Root Cause Analysis (Occurance)
Why 1 Wrong parts dispatch 520HQ00502 instead of 520HQ00202
Why 2 Wrong box pic during dispatch to ETL
Why 3 Loading helper did not check box according to invoice
Why 4 Loading helper did not aware about part number and models also
Why 5 On job training not done
Root Cause (Occurance) On job training not done
 
Root Cause Analysis (Outflow)
Why 1 Orfice valve 520HQ00202 NG observed at customer end
Why 2 Only sampling number of box verification done at logistics end
Why 3 box qty is not effetive to detect the problem
Why 4 Pass to customer
Why 5
Root Cause (Outflow) Stock details not veified
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceOn job training doneAmol08/02/2024Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System No
Change Details Daily stocks details verify share with Arvind & ETL
Inspection Method Other
Other Inspection Method Manual
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
10. Evidance of Countermeasure
Occurance (Before) Onjob training not done
674_Occurance_Before.jpeg
Occurance (After) Onjob training not done
674_Occurance_After.jpeg
Outflow (Before) Daily stock details not verify
674_Outflow_Before.jpg
Outflow (After) Daily stocks details verified and shared with Arvind and ETL
674_Outflow_After.jpg
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant Daily stock details verified for each models
 
12. Document Review
Documents PackingStd
Specify Other Document PACKING STANDARD
 
13. Effectiveness Of Action
Reviewed Quantity 20000
Reason for submission Next lot material observed to be Ok as Per Invoice.