QFR No - 8000863411
Defect Details
NC No. 8000863411
NC Date 17/02/2024
NC Submission Date
Part No. 520FG07802
Part Name GEAR PRIMARY DRIVEN (JZ)
Supplier Name & Code 200172-AURANGABAD AUTO ENGG PVT LTD
ETL Plant 1132-ETL K-226/1 TRANSMISSION
Defect Details PATCH MARK ON FACE.-DFC OBS 0.12 AGAINST 0.07
 
1. Problem Description
Defect Description Flicker observed excess up to 0.030 mm against 0.010 mm -DFCE observed 0.12 mm against 0.040 mm
Detection Stage Receipt
Problem Severity Function
NG Quantity 1
Is Defect Repeatative? Yes
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID verma.aaepl@gmail.com
Plant Head/CEO Email ID aaepl.pantnagar@sangkaj.com
MD Email ID steel@sangkaj.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
1565
0
0
1008
1890
4463
Check Qty
1565
0
0
1008
1890
4463
NG Qty
25
0
0
12
7
44
 
Scrap 0
Rework 44
Under Deviation 0
Containment Action
All WIP 100% Rechecked
 
3. Process Flow
Process Flow Description
CNC Blank Inward---Hobbing ---HT--- ID Honing---Teeth Honing -----Final Inspection ----Oiling Packing ---Dispatch
 
4. Process Details
Process / Operation Teeth Honing
Outsource Yes
Machine / Cell Teeth Honing Machine
Machine / Cell No. HMX 260
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MaterialLess Allowance for teeth HoningLess allowance for teeth honingO
 
6. Inspection Method Analysis (Current)
Inspection Method Other
Other Inspection Method visual inspection
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
7. Root Cause Analysis (Occurance)
Why 1 Patch mark on teeth
Why 2 less material removal on teeth honing operation
Why 3 As per process requirement no sufficient stock for teeth honing
Why 4 Teeth honing input material face runout excess due to part excess bend in HT process
Why 5 HT charge making fixture bend & Crack
Root Cause (Occurance) HT charge making fixture bend & Crack
 
Root Cause Analysis (Outflow)
Why 1 Patch mark on teeth
Why 2 Part detected in final inspection
Why 3 less awareness of final inspector
Why 4 N/A
Why 5 N/A
Root Cause (Outflow) Less awareness of final inspector
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceNew HT charge making plate orderedMr.Raut20/03/2024Pending
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details 1) Training provided to all final inspector 2) Ok Not Ok part OPL displayed at final inspection 3) Before teeth honing 100% face runout inspection started .
Inspection Method Other
Other Inspection Method Visual Inspection
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
10. Evidance of Countermeasure
Occurance (Before) Evidence attached
684_Occurance_Before.xlsx
Occurance (After) Evidence attached
684_Occurance_After.xlsx
Outflow (Before) Evidence attached
684_Outflow_Before.xlsx
Outflow (After) Evidence attached
684_Outflow_After.xlsx
 
11. Horizontal Deployment
Horizontal Deployment Required No
Applicable Machine / Model / Plant N/A
 
12. Document Review
Documents ControlPlan, WISOP, AuditCheckSheet, InspCheckSheet
Specify Other Document No
 
13. Effectiveness Of Action
Reviewed Quantity
Reason for submission