QFR No - 8000863411
Defect Details
NC No. | 8000863411 |
NC Date | 17/02/2024 |
NC Submission Date | |
Part No. | 520FG07802 |
Part Name | GEAR PRIMARY DRIVEN (JZ) |
Supplier Name & Code | 200172-AURANGABAD AUTO ENGG PVT LTD |
ETL Plant | 1132-ETL K-226/1 TRANSMISSION |
Defect Details | PATCH MARK ON FACE.-DFC OBS 0.12 AGAINST 0.07 |
1. Problem Description
Defect Description | Flicker observed excess up to 0.030 mm against 0.010 mm -DFCE observed 0.12 mm against 0.040 mm |
Detection Stage | Receipt |
Problem Severity | Function |
NG Quantity | 1 |
Is Defect Repeatative? | Yes |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | verma.aaepl@gmail.com |
Plant Head/CEO Email ID | aaepl.pantnagar@sangkaj.com |
MD Email ID | steel@sangkaj.com |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
1565
|
0
|
0
|
1008
|
1890
|
4463
|
Check Qty |
1565
|
0
|
0
|
1008
|
1890
|
4463
|
NG Qty |
25
|
0
|
0
|
12
|
7
|
44
|
Scrap | 0 |
Rework | 44 |
Under Deviation | 0 |
Containment Action |
---|
All WIP 100% Rechecked |
3. Process Flow
Process Flow Description |
---|
CNC Blank Inward---Hobbing ---HT--- ID Honing---Teeth Honing -----Final Inspection ----Oiling Packing ---Dispatch |
4. Process Details
Process / Operation | Teeth Honing |
Outsource | Yes |
Machine / Cell | Teeth Honing Machine |
Machine / Cell No. | HMX 260 |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Material | Less Allowance for teeth Honing | Less allowance for teeth honing | O |
6. Inspection Method Analysis (Current)
Inspection Method | Other |
Other Inspection Method | visual inspection |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100% |
7. Root Cause Analysis (Occurance)
Why 1 | Patch mark on teeth |
Why 2 | less material removal on teeth honing operation |
Why 3 | As per process requirement no sufficient stock for teeth honing |
Why 4 | Teeth honing input material face runout excess due to part excess bend in HT process |
Why 5 | HT charge making fixture bend & Crack |
Root Cause (Occurance) | HT charge making fixture bend & Crack |
Root Cause Analysis (Outflow)
Why 1 | Patch mark on teeth |
Why 2 | Part detected in final inspection |
Why 3 | less awareness of final inspector |
Why 4 | N/A |
Why 5 | N/A |
Root Cause (Outflow) | Less awareness of final inspector |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Occurance | New HT charge making plate ordered | Mr.Raut | 20/03/2024 | Pending |
9. Inspection Method After Customer Complaint
Change In Inspection System | Yes |
Change Details | 1) Training provided to all final inspector 2) Ok Not Ok part OPL displayed at final inspection 3) Before teeth honing 100% face runout inspection started . |
Inspection Method | Other |
Other Inspection Method | Visual Inspection |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100% |
10. Evidance of Countermeasure
Occurance (Before) |
Evidence attached 684_Occurance_Before.xlsx |
Occurance (After) |
Evidence attached 684_Occurance_After.xlsx |
Outflow (Before) |
Evidence attached 684_Outflow_Before.xlsx |
Outflow (After) |
Evidence attached 684_Outflow_After.xlsx |
11. Horizontal Deployment
Horizontal Deployment Required | No |
Applicable Machine / Model / Plant | N/A |
12. Document Review
Documents | ControlPlan, WISOP, AuditCheckSheet, InspCheckSheet |
Specify Other Document | No |
13. Effectiveness Of Action
Reviewed Quantity | |
Reason for submission |