QFR No - 8000865087
Defect Details
NC No. 8000865087
NC Date 29/02/2024
NC Submission Date
Part No. B2BK06823O
Part Name CALIPER BODY-PAINTED - ATHER FR
Supplier Name & Code 206460-TULJA ENTERPRISES
ETL Plant 1120-ETL K-226/2 Disc Brakes
Defect Details POWDER COATING NOT OK-AFTER 100% INSP. POWDER COATING UNCOVER,
 
1. Problem Description
Defect Description POWDER COATING NOT OK-AFTER 100% INSP. POWDER COATING UNCOVER,
Detection Stage Receipt
Problem Severity Aesthetic
NG Quantity 217
Is Defect Repeatative? Yes
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID quality.tulja@gmail.com
Plant Head/CEO Email ID tuljaenterprises.e124@gmail.com
MD Email ID tuljaenterprises.e124@gmail.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
15126
0
0
0
0
15126
Check Qty
1363
0
0
0
0
1363
NG Qty
217
0
0
0
0
217
 
Scrap 0
Rework 217
Under Deviation 0
Containment Action
Given training to painter how paint critical area during painting process.
 
3. Process Flow
Process Flow Description
Inward Inspection-PT process-WDO-PC-Baking-Final Inspection-Packing & Dispatch
 
4. Process Details
Process / Operation Coating
Outsource No
Machine / Cell Wagner coating Gun
Machine / Cell No. 01
5. Problem Analysis
Type Possible Cause Fact Verification Jud
ManUnskilled operatoerdue to unskilled operatorO
 
6. Inspection Method Analysis (Current)
Inspection Method Other
Other Inspection Method Visual
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
7. Root Cause Analysis (Occurance)
Why 1 During coating skip critical area.
Why 2 No awareness to operator about how to cover all critical area by coating.
Why 3 Skill level 2 operator was appointed
Why 4 Unskilled operator
Why 5
Root Cause (Occurance) Unskilled operator
 
Root Cause Analysis (Outflow)
Why 1 NG material mix up in Finish Good.
Why 2 Both location was near each other
Why 3
Why 4
Why 5
Root Cause (Outflow) OK/Not OK material mix up
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceGiven training to coating operator for critical parts areaproduction /Quality05/03/202405/03/2024Completed
OutflowDefine OK/Not OK material location away from each other.Prod.& Inspector04/03/202404/03/2024Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System No
Change Details No change required,due to mix up by loading person.
Inspection Method Other
Other Inspection Method Visual
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
10. Evidance of Countermeasure
Occurance (Before) Skill level 2 operator
697_Occurance_Before.xlsx
Occurance (After) Given training to operator
697_Occurance_After.pdf
Outflow (Before) OK/Not OK material location near each other
697_Outflow_Before.xlsx
Outflow (After) Define OK/Not OK location
697_Outflow_After.xlsx
 
11. Horizontal Deployment
Horizontal Deployment Required No
Applicable Machine / Model / Plant NA
 
12. Document Review
Documents
Specify Other Document NA
 
13. Effectiveness Of Action
Reviewed Quantity
Reason for submission