QFR No - 8000865087
Defect Details
NC No. | 8000865087 |
NC Date | 29/02/2024 |
NC Submission Date | |
Part No. | B2BK06823O |
Part Name | CALIPER BODY-PAINTED - ATHER FR |
Supplier Name & Code | 206460-TULJA ENTERPRISES |
ETL Plant | 1120-ETL K-226/2 Disc Brakes |
Defect Details | POWDER COATING NOT OK-AFTER 100% INSP. POWDER COATING UNCOVER, |
1. Problem Description
Defect Description | POWDER COATING NOT OK-AFTER 100% INSP. POWDER COATING UNCOVER, |
Detection Stage | Receipt |
Problem Severity | Aesthetic |
NG Quantity | 217 |
Is Defect Repeatative? | Yes |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | quality.tulja@gmail.com |
Plant Head/CEO Email ID | tuljaenterprises.e124@gmail.com |
MD Email ID | tuljaenterprises.e124@gmail.com |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
15126
|
0
|
0
|
0
|
0
|
15126
|
Check Qty |
1363
|
0
|
0
|
0
|
0
|
1363
|
NG Qty |
217
|
0
|
0
|
0
|
0
|
217
|
Scrap | 0 |
Rework | 217 |
Under Deviation | 0 |
Containment Action |
---|
Given training to painter how paint critical area during painting process. |
3. Process Flow
Process Flow Description |
---|
Inward Inspection-PT process-WDO-PC-Baking-Final Inspection-Packing & Dispatch |
4. Process Details
Process / Operation | Coating |
Outsource | No |
Machine / Cell | Wagner coating Gun |
Machine / Cell No. | 01 |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Man | Unskilled operatoer | due to unskilled operator | O |
6. Inspection Method Analysis (Current)
Inspection Method | Other |
Other Inspection Method | Visual |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100% |
7. Root Cause Analysis (Occurance)
Why 1 | During coating skip critical area. |
Why 2 | No awareness to operator about how to cover all critical area by coating. |
Why 3 | Skill level 2 operator was appointed |
Why 4 | Unskilled operator |
Why 5 | |
Root Cause (Occurance) | Unskilled operator |
Root Cause Analysis (Outflow)
Why 1 | NG material mix up in Finish Good. |
Why 2 | Both location was near each other |
Why 3 | |
Why 4 | |
Why 5 | |
Root Cause (Outflow) | OK/Not OK material mix up |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Occurance | Given training to coating operator for critical parts area | production /Quality | 05/03/2024 | 05/03/2024 | Completed |
Outflow | Define OK/Not OK material location away from each other. | Prod.& Inspector | 04/03/2024 | 04/03/2024 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | No |
Change Details | No change required,due to mix up by loading person. |
Inspection Method | Other |
Other Inspection Method | Visual |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100% |
10. Evidance of Countermeasure
Occurance (Before) |
Skill level 2 operator 697_Occurance_Before.xlsx |
Occurance (After) |
Given training to operator 697_Occurance_After.pdf |
Outflow (Before) |
OK/Not OK material location near each other 697_Outflow_Before.xlsx |
Outflow (After) |
Define OK/Not OK location 697_Outflow_After.xlsx |
11. Horizontal Deployment
Horizontal Deployment Required | No |
Applicable Machine / Model / Plant | NA |
12. Document Review
Documents | |
Specify Other Document | NA |
13. Effectiveness Of Action
Reviewed Quantity | |
Reason for submission |