QFR No - 8000867015
Defect Details
NC No. 8000867015
NC Date 13/03/2024
NC Submission Date
Part No. 550DZ05202
Part Name FORK BOLT :PRFH-006
Supplier Name & Code 101263-SINGLA PRECISION SCREWS
ETL Plant 1116-ETL K-120 Suspension
Defect Details NOT AS PER SPECIFICATION-AFTER ASSLY LEAKAGE FOUND
 
1. Problem Description
Defect Description Fork bolt Oil Leakage through Blow hole
Detection Stage Inprocess
Problem Severity Function
NG Quantity 2
Is Defect Repeatative? No
Defect Sketch / Photo vzrcupqzjwcvo04yu3ocopnr.png
Supplier Communication Details
Quality Head Email ID quality@singlaprecision.com
Plant Head/CEO Email ID quality@singlaprecision.com
MD Email ID aditya@singlaprecision.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
7000
0
0
0
0
7000
Check Qty
7000
0
0
0
0
7000
NG Qty
2
0
0
0
0
2
 
Scrap 2
Rework 0
Under Deviation 0
Containment Action
stocks checked 100% material All stage but no any part get this types
 
3. Process Flow
Process Flow Description
1-R/M ,2-PART OFF ,3-TAPPING 4-RE-TAPPING ,5-FLAT BUFFING IF NECESSARY ,6-THREAD ROLLING ,7-SURFACE TREATMENT ,8-FINAL INSPECTION 9-PAACKING
 
4. Process Details
Process / Operation RAW MATERIAL GRAIN FLOW OVER SIZE
Outsource Yes
Machine / Cell RAW MATERIAL
Machine / Cell No. N/A
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MachineDRILL DEPTH OVER SIZEVALIDATED AND FOUND OKO
MethodINSPECTION PLAN NOT EFFECTIVEVALIDATED AND FOUND INSPECTION PLAN NOT EFFECTIVE SO PART SKIPPED FROM FINAL INSPECTIONX
ManUNAWARENESS OF OPERATORVALIDATED AND FOUND OKO
MaterialRAW MATERIAL MIX -UP OTHER NG MATERIALVALIDATED AND FOUND NG MATERIAL MIX UPX
 
6. Inspection Method Analysis (Current)
Inspection Method Other
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size SAMPL PLAN
7. Root Cause Analysis (Occurance)
Why 1 NOT AS PER SPECIFICATION-AFTER ASSLY LEAKAGE FOUND
Why 2 RAW MATERIAL GRAIN FLOW OVER SIZE
Why 3 HOLD RAW MATERIAL MIX-UP OK MATERIAL
Why 4
Why 5
Root Cause (Occurance) HOLD RAW MATERIAL MIX-UP OK MATERIAL
 
Root Cause Analysis (Outflow)
Why 1 NOT AS PER SPECIFICATION-AFTER ASSLY LEAKAGE FOUND
Why 2 INSPECTION PLAN WAS NOT EFFECTIVE
Why 3 NG PART SKIPPED FROM INSPECTION
Why 4 SO NG PART DELIEVERED TO CUSTOMER
Why 5
Root Cause (Outflow) INSPECTION PLAN WAS NOT EFFECTIVE
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OutflowINSPECTION FREQUENCY CHANGE TO 100%GANESH MAURYA31/03/202431/03/2024Completed
OccuranceNG MATERIAL RED PAINT MARKGANESH MAURYA31/03/202431/03/2024Completed
OutflowFIFO SYSTEM MAINTAIN IN RAW MATERIAL STAGEGANESH MAURYA31/03/202431/03/2024Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details 100 % MATERIAL CHECKED
Inspection Method Other
Other Inspection Method R/M GRAIN FLOW CHECK
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
10. Evidance of Countermeasure
Occurance (Before) BRFORE REJECTION RED PAINT MARK NOT AVAILABLE
710_Occurance_Before.xlsx
Occurance (After) AFTER REJECTION RED PAINT MARK AVAILABLE
710_Occurance_After.xlsx
Outflow (Before) BEFORE - INSPECTION AS PER SAMPLING PLAN
710_Outflow_Before.xlsx
Outflow (After) AFTER - 100% CHECKED MATERIAL
710_Outflow_After.xlsx
 
11. Horizontal Deployment
Horizontal Deployment Required No
Applicable Machine / Model / Plant FORK BOLT (PRFH-006/K23A)
 
12. Document Review
Documents ControlPlan, WISOP
Specify Other Document NO
 
13. Effectiveness Of Action
Reviewed Quantity 15
Reason for submission Rejection material identification started. WI required.