QFR No - 8000867378
Defect Details
NC No. 8000867378
NC Date 18/03/2024
NC Submission Date
Part No. 520PP01902
Part Name WHEEL CLUTCH FINISHED UPGRADE
Supplier Name & Code 100656-MADHURA DIE CAST PVT.LTD
ETL Plant 1132-ETL K-226/1 TRANSMISSION
Defect Details CRACK-OD CRACK ISSUE
 
1. Problem Description
Defect Description Crack Issue observed on OD Ø110±0.3 mm
Detection Stage Receipt
Problem Severity Function
NG Quantity 28
Is Defect Repeatative? No
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID madhuradiecast@gmail.com
Plant Head/CEO Email ID madhuradiecast@gmail.com
MD Email ID madhuradiecast@gaikegroup.in
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
3384
2000
0
0
0
5384
Check Qty
3384
2000
0
0
0
5384
NG Qty
32
35
0
0
0
67
 
Scrap 67
Rework 0
Under Deviation 0
Containment Action
1. 100% material of the 3W4S Wheel segregation done at the customer end. 2.. Started 100% of the visual checking of the crack on the OD. And Started 100% of the marking on the OD of the Components.
 
3. Process Flow
Process Flow Description
1. Casting 2. Fettling 3. CNC 1st Set-up 4. CNC 2nd Set-up 5.Drilling & Tapping 6.Final Inspection
 
4. Process Details
Process / Operation Casting
Outsource No
Machine / Cell HPDC MC
Machine / Cell No. 02
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MaterialDie material was not ok.Check and verify found okO
MachineDie was OverlockVerified & Found OKO
ToolDie life was completedFound Not OKX
 
6. Inspection Method Analysis (Current)
Inspection Method Instrument
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 1:1
7. Root Cause Analysis (Occurance)
Why 1 A crack was found on the OD 110.00mm.
Why 2 The casting ejection was uneven due to which parts got cracked.
Why 3 The running die moving side insert M1 was cracked at various points.
Why 4 Die life was completed of M1 die. And the new die was under approval.
Why 5
Root Cause (Occurance) Die life was completed of M1 die.
 
Root Cause Analysis (Outflow)
Why 1 This micro-crack part was visually not arrested on the final inspection table
Why 2 Micro crack was not visible without a magnifying glass.
Why 3
Why 4
Why 5
Root Cause (Outflow) Micro crack was not visible without a magnifying glass.
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceThe old die (M1) was scrapped and the new die (M2) was implemented for the production.Production supervisior20/03/202418/03/2024Completed
Outflow1. Training and awareness were given to the Final inspector about the Visual checking of the Crack on the OD 110.00mm. 2. The magnified glass is implemented on the final inspection table for the visual checking of the micro cracks on the OD of the parts. 3. OPL is displayed.QA Supervisor15/03/202416/03/2024Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details The magnified glass is implemented on the final inspection table for the visual checking of the micro cracks on the OD of the parts.
Inspection Method Instrument
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 1:1
10. Evidance of Countermeasure
Occurance (Before) The running die moving side insert M1 was cracked
714_Occurance_Before.jpeg
Occurance (After) A new die (M2) was implemented for the production.
714_Occurance_After.jpeg
Outflow (Before) Micro crack was not visible without magnifying glass.
714_Outflow_Before.jpeg
Outflow (After) The magnified glass is implemented on the final inspection table for the visual checking of the micro-cracks on the OD of the parts.
714_Outflow_After.jpeg
 
11. Horizontal Deployment
Horizontal Deployment Required No
Applicable Machine / Model / Plant NO
 
12. Document Review
Documents InspCheckSheet
Specify Other Document NA
 
13. Effectiveness Of Action
Reviewed Quantity 2000
Reason for submission OK