QFR No - 8000868409
Defect Details
NC No. | 8000868409 |
NC Date | 22/03/2024 |
NC Submission Date | |
Part No. | F2GN12502B |
Part Name | MAIN SPRING J1A & J1D |
Supplier Name & Code | 100180-BHALLA TECHTRAN INDUSTRIES LIM |
ETL Plant | 1117-ETL K-228/9 Suspension |
Defect Details | NOT AS PER SPECIFICATION-PARELLELISM MORE |
1. Problem Description
Defect Description | PARELLELISM MORE |
Detection Stage | Inprocess |
Problem Severity | Function |
NG Quantity | 91 |
Is Defect Repeatative? | Yes |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | sunilaggarwal.btl@gmail.com |
Plant Head/CEO Email ID | plant1@btlsprings.com |
MD Email ID | amitbhalla.btl@gmail.com |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
2000
|
4500
|
4000
|
2000
|
0
|
12500
|
Check Qty |
2000
|
4500
|
0
|
2000
|
0
|
8500
|
NG Qty |
91
|
60
|
0
|
0
|
0
|
151
|
Scrap | 0 |
Rework | 151 |
Under Deviation | 0 |
Containment Action |
---|
Check the all material lying at ETL end and warehouse as well as inhouse |
3. Process Flow
Process Flow Description |
---|
RM Receipt & Inspection Coiling Stress relieving 1st End Grinding Shot Peening Stress relieving 2nd Scragging Final Inspection Packing & Dispatch |
4. Process Details
Process / Operation | End Grinding |
Outsource | No |
Machine / Cell | CNC Grinding |
Machine / Cell No. | WNJ Grinding m/c |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Material | Wrong material grade used | Verify and found OK as per Drg. | O |
Method | Grinding wheel dressing not as per decided freq. | Check wheel dressing record as per decided freq. | O |
Tool | Grinding plate as per requirement | Found old grinding plate with hole size more | X |
Man | New/Untrained operator | Verify operator skill matrix and found OK | O |
Method | Grinding wheel alignment not ok | Check wheel alignment with block | O |
Machine | Grinding feed more in programming | Verify and found OK | O |
6. Inspection Method Analysis (Current)
Inspection Method | Instrument |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | Sampling |
Sampling | No |
Sample Size | 05 Nos/Lot |
7. Root Cause Analysis (Occurance)
Why 1 | Parallelism out of specification |
Why 2 | End grinding was in taper |
Why 3 | More clearance in grinding plate hole w.r.t. spring OD |
Why 4 | Old grinding plate used with hole size more |
Why 5 | No identification on grinding plate |
Root Cause (Occurance) | Old grinding plate with hole size more used during grinding operation due to no identification on grinding plates |
Root Cause Analysis (Outflow)
Why 1 | Parallelism out of specification |
Why 2 | Not detect during PDI |
Why 3 | Sampling Inspection |
Why 4 | As per decided freq. |
Why 5 | |
Root Cause (Outflow) | Defected parts not detect during PDI inspection due to sampling inspection |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Occurance | Identify the grinding plates with No. and monthly validation started | Rajesh Choudhary | 28/03/2024 | 28/03/2024 | Completed |
Occurance | Grinding plate hole size check point added in setup approval and in process inspection check sheet and verified by Q.C. | Rajesh Choudhary | 27/03/2024 | 28/03/2024 | Completed |
Occurance | Separate racks made for storage of grinding plates with proper identification | Saudagar Prasad | 28/03/2024 | 28/03/2024 | Completed |
Outflow | Sampling freq. increased in PDI stage (05 nos from each crates in place of 05 nos/lot) | Rajesh Choudhary | 27/03/2024 | 28/03/2024 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | Yes |
Change Details | Checking freq. increased in PDI stage |
Inspection Method | Instrument |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | Sampling |
Sampling | No |
Sample Size | 05 Nos/Bin |
10. Evidance of Countermeasure
Occurance (Before) |
Unidentified grinding plate 725_Occurance_Before.jpg |
Occurance (After) |
OPL displayed and provide training to all concerned 725_Occurance_After.pdf |
Outflow (Before) |
Less sampling freq. 725_Outflow_Before.xls |
Outflow (After) |
Sampling freq. increased and revised control plan 725_Outflow_After.xls |
11. Horizontal Deployment
Horizontal Deployment Required | Yes |
Applicable Machine / Model / Plant | All main spring in grinding operation |
12. Document Review
Documents | ControlPlan, PFMEA, WISOP, InspCheckSheet |
Specify Other Document | OPL |
13. Effectiveness Of Action
Reviewed Quantity | 240 |
Reason for submission | Found ok |