QFR No - 8000868409
Defect Details
NC No. 8000868409
NC Date 22/03/2024
NC Submission Date
Part No. F2GN12502B
Part Name MAIN SPRING J1A & J1D
Supplier Name & Code 100180-BHALLA TECHTRAN INDUSTRIES LIM
ETL Plant 1117-ETL K-228/9 Suspension
Defect Details NOT AS PER SPECIFICATION-PARELLELISM MORE
 
1. Problem Description
Defect Description PARELLELISM MORE
Detection Stage Inprocess
Problem Severity Function
NG Quantity 91
Is Defect Repeatative? Yes
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID sunilaggarwal.btl@gmail.com
Plant Head/CEO Email ID plant1@btlsprings.com
MD Email ID amitbhalla.btl@gmail.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
2000
4500
4000
2000
0
12500
Check Qty
2000
4500
0
2000
0
8500
NG Qty
91
60
0
0
0
151
 
Scrap 0
Rework 151
Under Deviation 0
Containment Action
Check the all material lying at ETL end and warehouse as well as inhouse
 
3. Process Flow
Process Flow Description
RM Receipt & Inspection Coiling Stress relieving 1st End Grinding Shot Peening Stress relieving 2nd Scragging Final Inspection Packing & Dispatch
 
4. Process Details
Process / Operation End Grinding
Outsource No
Machine / Cell CNC Grinding
Machine / Cell No. WNJ Grinding m/c
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MaterialWrong material grade usedVerify and found OK as per Drg.O
MethodGrinding wheel dressing not as per decided freq.Check wheel dressing record as per decided freq.O
ToolGrinding plate as per requirementFound old grinding plate with hole size moreX
ManNew/Untrained operatorVerify operator skill matrix and found OKO
MethodGrinding wheel alignment not okCheck wheel alignment with blockO
MachineGrinding feed more in programmingVerify and found OKO
 
6. Inspection Method Analysis (Current)
Inspection Method Instrument
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size 05 Nos/Lot
7. Root Cause Analysis (Occurance)
Why 1 Parallelism out of specification
Why 2 End grinding was in taper
Why 3 More clearance in grinding plate hole w.r.t. spring OD
Why 4 Old grinding plate used with hole size more
Why 5 No identification on grinding plate
Root Cause (Occurance) Old grinding plate with hole size more used during grinding operation due to no identification on grinding plates
 
Root Cause Analysis (Outflow)
Why 1 Parallelism out of specification
Why 2 Not detect during PDI
Why 3 Sampling Inspection
Why 4 As per decided freq.
Why 5
Root Cause (Outflow) Defected parts not detect during PDI inspection due to sampling inspection
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceIdentify the grinding plates with No. and monthly validation startedRajesh Choudhary28/03/202428/03/2024Completed
OccuranceGrinding plate hole size check point added in setup approval and in process inspection check sheet and verified by Q.C.Rajesh Choudhary27/03/202428/03/2024Completed
OccuranceSeparate racks made for storage of grinding plates with proper identificationSaudagar Prasad28/03/202428/03/2024Completed
OutflowSampling freq. increased in PDI stage (05 nos from each crates in place of 05 nos/lot)Rajesh Choudhary27/03/202428/03/2024Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details Checking freq. increased in PDI stage
Inspection Method Instrument
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size 05 Nos/Bin
10. Evidance of Countermeasure
Occurance (Before) Unidentified grinding plate
725_Occurance_Before.jpg
Occurance (After) OPL displayed and provide training to all concerned
725_Occurance_After.pdf
Outflow (Before) Less sampling freq.
725_Outflow_Before.xls
Outflow (After) Sampling freq. increased and revised control plan
725_Outflow_After.xls
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant All main spring in grinding operation
 
12. Document Review
Documents ControlPlan, PFMEA, WISOP, InspCheckSheet
Specify Other Document OPL
 
13. Effectiveness Of Action
Reviewed Quantity 240
Reason for submission Found ok