QFR No - 8000870319
Defect Details
NC No. 8000870319
NC Date 05/04/2024
NC Submission Date
Part No. 550LG06702
Part Name SEAT PIPE-(HMS-30 & HMP-30)
Supplier Name & Code 100929-HARSHAD ENGINEERING COMPANY
ETL Plant 1143-ETL Suspension Halol, Vadodara
Defect Details THREADING NOT OK-HALF THREAD
 
1. Problem Description
Defect Description SEAT PIPE M8 X 1.25 -6G HALF THREAD FOUND AGAINST 14 MIN. REQUIRED
Detection Stage Inprocess
Problem Severity Fitment
NG Quantity 1
Is Defect Repeatative? Yes
Defect Sketch / Photo 3msmklh13r5mlf2ikgv3wqbt.jpg
Supplier Communication Details
Quality Head Email ID qaharshad@miteshauto.com
Plant Head/CEO Email ID sjkadam@miteshauto.com
MD Email ID auto.mitesh@gmail.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
4100
0
0
7100
4250
15450
Check Qty
4100
0
0
7100
4250
15450
NG Qty
4
0
0
0
0
4
 
Scrap 4
Rework 0
Under Deviation 0
Containment Action
100 % sorting done for ETL End, HEC WIP & FG material
 
3. Process Flow
Process Flow Description
Cutting-Draw-Forging(Head Formation)-Rough Grinding-CNC (Head, Boring & Tapping)-Punching-Finish Grinding-Final Inspection-Packing-Dispatch
 
4. Process Details
Process / Operation Tapping
Outsource No
Machine / Cell Tapping
Machine / Cell No. SPM2
5. Problem Analysis
Type Possible Cause Fact Verification Jud
ToolNANAX
MachineLimit switch malfunctionObserved Limit switch MalfunctionO
ManNANAX
MethodNANAX
 
6. Inspection Method Analysis (Current)
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size IS2500
7. Root Cause Analysis (Occurance)
Why 1 Tap not perform for complete threading length
Why 2 Tap not insert/Pass up to full length
Why 3 Tapping unit not work up to decided 15.0mm length
Why 4 At tapping operation station limit switch malfunction happen
Why 5 Limit switch malfunction happen
Root Cause (Occurance) Limit switch malfunction happen
 
Root Cause Analysis (Outflow)
Why 1 Half Threading
Why 2 after tapping operation parts are checked on sampling basis
Why 3 From initial stage it is carried out
Why 4 Skip from Final Inspection
Why 5 Not detected
Root Cause (Outflow) Not detected
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceLimit switch malfunction happenD.D. Jopale28/04/202410/04/2024Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System No
Change Details No Change, Inspection freq. Double
Inspection Method Other
Other Inspection Method Visual Inspection
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100 %
10. Evidance of Countermeasure
Occurance (Before) Limit switch malfunction while operating
730_Occurance_Before.jpg
Occurance (After) Limit switch replace by new one
730_Occurance_After.jpg
Outflow (Before) Parts checked for tapping presence
730_Outflow_Before.jpg
Outflow (After) Parts checked to ensure complete tapping
730_Outflow_After.jpg
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant All SPM & Tapping Machines
 
12. Document Review
Documents ControlPlan
Specify Other Document NA
 
13. Effectiveness Of Action
Reviewed Quantity
Reason for submission