QFR No - 8000870319
Defect Details
NC No. | 8000870319 |
NC Date | 05/04/2024 |
NC Submission Date | |
Part No. | 550LG06702 |
Part Name | SEAT PIPE-(HMS-30 & HMP-30) |
Supplier Name & Code | 100929-HARSHAD ENGINEERING COMPANY |
ETL Plant | 1143-ETL Suspension Halol, Vadodara |
Defect Details | THREADING NOT OK-HALF THREAD |
1. Problem Description
Defect Description | SEAT PIPE M8 X 1.25 -6G HALF THREAD FOUND AGAINST 14 MIN. REQUIRED |
Detection Stage | Inprocess |
Problem Severity | Fitment |
NG Quantity | 1 |
Is Defect Repeatative? | Yes |
Defect Sketch / Photo | 3msmklh13r5mlf2ikgv3wqbt.jpg |
Supplier Communication Details
Quality Head Email ID | qaharshad@miteshauto.com |
Plant Head/CEO Email ID | sjkadam@miteshauto.com |
MD Email ID | auto.mitesh@gmail.com |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
4100
|
0
|
0
|
7100
|
4250
|
15450
|
Check Qty |
4100
|
0
|
0
|
7100
|
4250
|
15450
|
NG Qty |
4
|
0
|
0
|
0
|
0
|
4
|
Scrap | 4 |
Rework | 0 |
Under Deviation | 0 |
Containment Action |
---|
100 % sorting done for ETL End, HEC WIP & FG material |
3. Process Flow
Process Flow Description |
---|
Cutting-Draw-Forging(Head Formation)-Rough Grinding-CNC (Head, Boring & Tapping)-Punching-Finish Grinding-Final Inspection-Packing-Dispatch |
4. Process Details
Process / Operation | Tapping |
Outsource | No |
Machine / Cell | Tapping |
Machine / Cell No. | SPM2 |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Tool | NA | NA | X |
Machine | Limit switch malfunction | Observed Limit switch Malfunction | O |
Man | NA | NA | X |
Method | NA | NA | X |
6. Inspection Method Analysis (Current)
Inspection Method | Gauge |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | Sampling |
Sampling | No |
Sample Size | IS2500 |
7. Root Cause Analysis (Occurance)
Why 1 | Tap not perform for complete threading length |
Why 2 | Tap not insert/Pass up to full length |
Why 3 | Tapping unit not work up to decided 15.0mm length |
Why 4 | At tapping operation station limit switch malfunction happen |
Why 5 | Limit switch malfunction happen |
Root Cause (Occurance) | Limit switch malfunction happen |
Root Cause Analysis (Outflow)
Why 1 | Half Threading |
Why 2 | after tapping operation parts are checked on sampling basis |
Why 3 | From initial stage it is carried out |
Why 4 | Skip from Final Inspection |
Why 5 | Not detected |
Root Cause (Outflow) | Not detected |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Occurance | Limit switch malfunction happen | D.D. Jopale | 28/04/2024 | 10/04/2024 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | No |
Change Details | No Change, Inspection freq. Double |
Inspection Method | Other |
Other Inspection Method | Visual Inspection |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100 % |
10. Evidance of Countermeasure
Occurance (Before) |
Limit switch malfunction while operating 730_Occurance_Before.jpg |
Occurance (After) |
Limit switch replace by new one 730_Occurance_After.jpg |
Outflow (Before) |
Parts checked for tapping presence 730_Outflow_Before.jpg |
Outflow (After) |
Parts checked to ensure complete tapping 730_Outflow_After.jpg |
11. Horizontal Deployment
Horizontal Deployment Required | Yes |
Applicable Machine / Model / Plant | All SPM & Tapping Machines |
12. Document Review
Documents | ControlPlan |
Specify Other Document | NA |
13. Effectiveness Of Action
Reviewed Quantity | |
Reason for submission |