QFR No - 8000871813
Defect Details
NC No. 8000871813
NC Date 19/04/2024
NC Submission Date
Part No. F1GN01102B
Part Name MAIN SPRING K86A
Supplier Name & Code 101236-SUMA SPRINGS PRIVATE LIMITED
ETL Plant 1146-ETL Suspension Narasapura
Defect Details DIAMETER OVER SIZE-OD MORE ISSUE
 
1. Problem Description
Defect Description K86 MAIN SPRING OD MORE ISSUE
Detection Stage Inprocess
Problem Severity Fitment
NG Quantity 6
Is Defect Repeatative? No
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID qc@sumasprings.com
Plant Head/CEO Email ID vp@sumasprings.com
MD Email ID
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
2000
0
0
7200
0
9200
Check Qty
2000
0
0
7200
0
9200
NG Qty
6
0
0
0
0
6
 
Scrap 6
Rework 0
Under Deviation 0
Containment Action
.Quality Alert prepared and awareness created among Internal CFT team (Production, QC/QA,Stores,Despatch,QC Inspectors) Segregation Process initiated at entire Pipeline to identify the NG part and to prevent the NG part to reach to customer
 
3. Process Flow
Process Flow Description
COIL+TEM+GRIN+SHOT+SCR+TEM+OILING +PACK+DESPATCH
 
4. Process Details
Process / Operation COILING
Outsource No
Machine / Cell COILING MACHINE
Machine / Cell No. COILING M/C
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MethodCoilingSet Setup part mix up during processO
MethodRandom sampling methodverified and found Sampling ineffectiveO
 
6. Inspection Method Analysis (Current)
Inspection Method Instrument
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size 10%
7. Root Cause Analysis (Occurance)
Why 1 OD more
Why 2 Set up part kept in the regular bin
Why 3 previous shift rejections not cleared
Why 4
Why 5
Root Cause (Occurance) previous shift rejections not cleared
 
Root Cause Analysis (Outflow)
Why 1 NG Parts Not found during PDI
Why 2 PDI done as per AOI
Why 3 PDI inspection not effective
Why 4
Why 5
Root Cause (Outflow) PDI inspection not effective
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceInstruction provided that Daily 4.30 Pm all rejections to be monitored and moved to scrap yard & Set up rejections only kept in the red binVinay11/04/2024Completed
OutflowSampling quantity % will be increase by 50% more than the existing lot qty at PDIMoulidharan10/04/202410/04/2024Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details Sampling quantity % will be increase by 50% more than the existing lot qty at PDI
Inspection Method Instrument
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size 50%
10. Evidance of Countermeasure
Occurance (Before) previous shift rejections not cleared
751_Occurance_Before.pdf
Occurance (After) Instruction provided that Daily 4.30 Pm all rejections to be monitored and moved to scrap yard & Set up rejections only kept in the red bin
751_Occurance_After.pdf
Outflow (Before) PDI inspection not effective
751_Outflow_Before.pdf
Outflow (After) Sampling quantity % will be increase by 50% more than the existing lot qty at PDI
751_Outflow_After.pdf
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant F1GN011020
 
12. Document Review
Documents
Specify Other Document Q_ alert - Scrap reg
 
13. Effectiveness Of Action
Reviewed Quantity
Reason for submission