QFR No - 8000871813
Defect Details
NC No. | 8000871813 |
NC Date | 19/04/2024 |
NC Submission Date | |
Part No. | F1GN01102B |
Part Name | MAIN SPRING K86A |
Supplier Name & Code | 101236-SUMA SPRINGS PRIVATE LIMITED |
ETL Plant | 1146-ETL Suspension Narasapura |
Defect Details | DIAMETER OVER SIZE-OD MORE ISSUE |
1. Problem Description
Defect Description | K86 MAIN SPRING OD MORE ISSUE |
Detection Stage | Inprocess |
Problem Severity | Fitment |
NG Quantity | 6 |
Is Defect Repeatative? | No |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | qc@sumasprings.com |
Plant Head/CEO Email ID | vp@sumasprings.com |
MD Email ID |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
2000
|
0
|
0
|
7200
|
0
|
9200
|
Check Qty |
2000
|
0
|
0
|
7200
|
0
|
9200
|
NG Qty |
6
|
0
|
0
|
0
|
0
|
6
|
Scrap | 6 |
Rework | 0 |
Under Deviation | 0 |
Containment Action |
---|
.Quality Alert prepared and awareness created among Internal CFT team (Production, QC/QA,Stores,Despatch,QC Inspectors) Segregation Process initiated at entire Pipeline to identify the NG part and to prevent the NG part to reach to customer |
3. Process Flow
Process Flow Description |
---|
COIL+TEM+GRIN+SHOT+SCR+TEM+OILING +PACK+DESPATCH |
4. Process Details
Process / Operation | COILING |
Outsource | No |
Machine / Cell | COILING MACHINE |
Machine / Cell No. | COILING M/C |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Method | Coiling | Set Setup part mix up during process | O |
Method | Random sampling method | verified and found Sampling ineffective | O |
6. Inspection Method Analysis (Current)
Inspection Method | Instrument |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | Sampling |
Sampling | No |
Sample Size | 10% |
7. Root Cause Analysis (Occurance)
Why 1 | OD more |
Why 2 | Set up part kept in the regular bin |
Why 3 | previous shift rejections not cleared |
Why 4 | |
Why 5 | |
Root Cause (Occurance) | previous shift rejections not cleared |
Root Cause Analysis (Outflow)
Why 1 | NG Parts Not found during PDI |
Why 2 | PDI done as per AOI |
Why 3 | PDI inspection not effective |
Why 4 | |
Why 5 | |
Root Cause (Outflow) | PDI inspection not effective |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Occurance | Instruction provided that Daily 4.30 Pm all rejections to be monitored and moved to scrap yard & Set up rejections only kept in the red bin | Vinay | 11/04/2024 | Completed | |
Outflow | Sampling quantity % will be increase by 50% more than the existing lot qty at PDI | Moulidharan | 10/04/2024 | 10/04/2024 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | Yes |
Change Details | Sampling quantity % will be increase by 50% more than the existing lot qty at PDI |
Inspection Method | Instrument |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | Sampling |
Sampling | No |
Sample Size | 50% |
10. Evidance of Countermeasure
Occurance (Before) |
previous shift rejections not cleared 751_Occurance_Before.pdf |
Occurance (After) |
Instruction provided that Daily 4.30 Pm all rejections to be monitored and moved to scrap yard & Set up rejections only kept in the red bin 751_Occurance_After.pdf |
Outflow (Before) |
PDI inspection not effective 751_Outflow_Before.pdf |
Outflow (After) |
Sampling quantity % will be increase by 50% more than the existing lot qty at PDI 751_Outflow_After.pdf |
11. Horizontal Deployment
Horizontal Deployment Required | Yes |
Applicable Machine / Model / Plant | F1GN011020 |
12. Document Review
Documents | |
Specify Other Document | Q_ alert - Scrap reg |
13. Effectiveness Of Action
Reviewed Quantity | |
Reason for submission |