QFR No - 8000872766
Defect Details
NC No. | 8000872766 |
NC Date | 02/05/2024 |
NC Submission Date | |
Part No. | S2KH01502B |
Part Name | REBOUND SPRING K55G |
Supplier Name & Code | 100185-HELICAL SPRINGS |
ETL Plant | 1136-ETL Suspension Sanand |
Defect Details | BEND-SHARP EDGE AND BEND |
1. Problem Description
Defect Description | Bend and sharp edge |
Detection Stage | Warranty |
Problem Severity | Function |
NG Quantity | 5 |
Is Defect Repeatative? | No |
Defect Sketch / Photo | sego1mwjmrqh0ahtoh5qj3yl.jpg |
Supplier Communication Details
Quality Head Email ID | Prabhat@helicalsprings.in |
Plant Head/CEO Email ID | awadhwa@helicalsprings.in |
MD Email ID | ataneja@helicalsprings.in |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
0
|
0
|
0
|
1200
|
0
|
1200
|
Check Qty |
0
|
0
|
0
|
1200
|
0
|
1200
|
NG Qty |
0
|
0
|
0
|
3
|
0
|
3
|
Scrap | 3 |
Rework | 0 |
Under Deviation | 0 |
Containment Action |
---|
all suspected material hold in Quarantine area for reverification |
3. Process Flow
Process Flow Description |
---|
Rm inspection -coiling - SR - Grinding - Sp- SR2-Scragging - surface treatment - pdi - packing - dispatch |
4. Process Details
Process / Operation | CNC grinding |
Outsource | No |
Machine / Cell | CNC Grinding |
Machine / Cell No. | N/A |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Method | Chamfer not available in guide plate | chamfer check & found not available | X |
Machine | Preventive maint not done | machine pm checked & found ok | O |
Man | Unskilled manpower | skill matrix checked & found | O |
Tool | Tool worn out | physically tool check & found ok | O |
Material | Rm not as per grade | Rm checked & found ok | O |
6. Inspection Method Analysis (Current)
Inspection Method | Gauge |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | Sampling |
Sampling | No |
Sample Size | 5 nos |
7. Root Cause Analysis (Occurance)
Why 1 | End coil bend in spring |
Why 2 | End Coil distorted during Grinding Process |
Why 3 | End coil stuck with guide plate in grinding process |
Why 4 | Level difference at junction of guide plate |
Why 5 | sharp corner observed at the edge of guide plate (entry ) |
Root Cause (Occurance) | sharp corner observed at the edge of guide plate (entry ) |
Root Cause Analysis (Outflow)
Why 1 | End Coil bend in spring |
Why 2 | Minor bend not detected at final stage |
Why 3 | |
Why 4 | |
Why 5 | |
Root Cause (Outflow) | Minor bend not detected at final stage |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Occurance | Limit sample displayed at WIP Area | Sunil | 30/04/2024 | Completed | |
Occurance | Training & awareness given to team | sonu upadhyay | 30/04/2024 | Completed | |
Outflow | 100 % inspection with Combination gauge OD & ID Both implemented in final stage | Sunil | 10/05/2024 | Completed | |
Occurance | Chamfer provided at sharp corner of guide plate to ensure smooth transition of spring from grinding wheel to guide plate | Arvind | 10/05/2024 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | Yes |
Change Details | 100 % inspection with combination gauge |
Inspection Method | Gauge |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100 % |
10. Evidance of Countermeasure
Occurance (Before) |
BEFORE - Chamfer not available in guide plate 772_Occurance_Before.xlsx |
Occurance (After) |
AFTER -Chamfer provided in Guide plate 772_Occurance_After.xlsx |
Outflow (Before) |
Before - Visual inspection 772_Outflow_Before.xlsx |
Outflow (After) |
after - Combination pin gauge used for inspection 772_Outflow_After.xlsx |
11. Horizontal Deployment
Horizontal Deployment Required | Yes |
Applicable Machine / Model / Plant | Model - k55 |
12. Document Review
Documents | ControlPlan, PFMEA, WISOP, ProcessFlowChart |
Specify Other Document | OPL,Training,Gauge |
13. Effectiveness Of Action
Reviewed Quantity | 5 |
Reason for submission | End coil bend in rebound spring K55 |