QFR No - 8000872766
Defect Details
NC No. 8000872766
NC Date 02/05/2024
NC Submission Date
Part No. S2KH01502B
Part Name REBOUND SPRING K55G
Supplier Name & Code 100185-HELICAL SPRINGS
ETL Plant 1136-ETL Suspension Sanand
Defect Details BEND-SHARP EDGE AND BEND
 
1. Problem Description
Defect Description Bend and sharp edge
Detection Stage Warranty
Problem Severity Function
NG Quantity 5
Is Defect Repeatative? No
Defect Sketch / Photo sego1mwjmrqh0ahtoh5qj3yl.jpg
Supplier Communication Details
Quality Head Email ID Prabhat@helicalsprings.in
Plant Head/CEO Email ID awadhwa@helicalsprings.in
MD Email ID ataneja@helicalsprings.in
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
0
0
0
1200
0
1200
Check Qty
0
0
0
1200
0
1200
NG Qty
0
0
0
3
0
3
 
Scrap 3
Rework 0
Under Deviation 0
Containment Action
all suspected material hold in Quarantine area for reverification
 
3. Process Flow
Process Flow Description
Rm inspection -coiling - SR - Grinding - Sp- SR2-Scragging - surface treatment - pdi - packing - dispatch
 
4. Process Details
Process / Operation CNC grinding
Outsource No
Machine / Cell CNC Grinding
Machine / Cell No. N/A
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MethodChamfer not available in guide platechamfer check & found not availableX
MachinePreventive maint not donemachine pm checked & found okO
ManUnskilled manpowerskill matrix checked & foundO
ToolTool worn outphysically tool check & found okO
MaterialRm not as per gradeRm checked & found okO
 
6. Inspection Method Analysis (Current)
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size 5 nos
7. Root Cause Analysis (Occurance)
Why 1 End coil bend in spring
Why 2 End Coil distorted during Grinding Process
Why 3 End coil stuck with guide plate in grinding process
Why 4 Level difference at junction of guide plate
Why 5 sharp corner observed at the edge of guide plate (entry )
Root Cause (Occurance) sharp corner observed at the edge of guide plate (entry )
 
Root Cause Analysis (Outflow)
Why 1 End Coil bend in spring
Why 2 Minor bend not detected at final stage
Why 3
Why 4
Why 5
Root Cause (Outflow) Minor bend not detected at final stage
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceLimit sample displayed at WIP AreaSunil30/04/2024Completed
OccuranceTraining & awareness given to teamsonu upadhyay30/04/2024Completed
Outflow100 % inspection with Combination gauge OD & ID Both implemented in final stageSunil10/05/2024Completed
OccuranceChamfer provided at sharp corner of guide plate to ensure smooth transition of spring from grinding wheel to guide plateArvind10/05/2024Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details 100 % inspection with combination gauge
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100 %
10. Evidance of Countermeasure
Occurance (Before) BEFORE - Chamfer not available in guide plate
772_Occurance_Before.xlsx
Occurance (After) AFTER -Chamfer provided in Guide plate
772_Occurance_After.xlsx
Outflow (Before) Before - Visual inspection
772_Outflow_Before.xlsx
Outflow (After) after - Combination pin gauge used for inspection
772_Outflow_After.xlsx
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant Model - k55
 
12. Document Review
Documents ControlPlan, PFMEA, WISOP, ProcessFlowChart
Specify Other Document OPL,Training,Gauge
 
13. Effectiveness Of Action
Reviewed Quantity 5
Reason for submission End coil bend in rebound spring K55