QFR No - 8000873485
Defect Details
NC No. 8000873485
NC Date 06/05/2024
NC Submission Date
Part No. F2LG03302B
Part Name SEAT PIPE (B104E
Supplier Name & Code 100648-JOTIBA TECHNOLOGIES PVT.LTD.
ETL Plant 1117-ETL K-228/9 Suspension
Defect Details NOT AS PER SPECIFICATION-GROOVE OD RUNOUT MORE
 
1. Problem Description
Defect Description GROOVE OD RUNOUT MORE
Detection Stage Receipt
Problem Severity Function
NG Quantity 52
Is Defect Repeatative? No
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID accjotiba@gmail.com
Plant Head/CEO Email ID sanghavi.rajesh@sanghavigroup.co.in
MD Email ID jotibatech@gmail.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
450
0
0
0
0
450
Check Qty
450
0
0
0
0
450
NG Qty
52
0
0
0
0
52
 
Scrap 52
Rework 0
Under Deviation 0
Containment Action
Boring set-up approval time inspect thread runout wrt groove diameter, if runout is ok then start boring operation.
 
3. Process Flow
Process Flow Description
10.Raw material Inspection ,20.Parting Off 30.Chamfer,40.Weighing,50.Draw Forging,60.Hex Forging,70.Rough Grinding,80.Collar Machining,90.Total length facing and Boring,100.Piercing,110.DF Hole chamfering,120. Compression Hole chamfering, 130.ID Reaming,140.Tapping,150.Finish Grinding,160.Final Inspection,170.ID Cleaning,180.Ultrasonic Cleaning,190.Apply antirust oil,200.Packing and Dispatch
 
4. Process Details
Process / Operation Total length facing and Boring
Outsource No
Machine / Cell CNC
Machine / Cell No. CNC01, CNC02, CNC05
5. Problem Analysis
Type Possible Cause Fact Verification Jud
ToolJob slip in holding split collet due to collet wear out.Collet condition is found ok.O
MachineAxial runout of job and spindle body above 0.1 mm.Found runout within 0.05 mmO
ManChuck jaw was break due to minor accident on machine.Operator not inspect jaw conditionX
MethodThread runout not inspect at boring setup approval time.Thread runout inspect at tapping operation done.X
MaterialBoring time ID runout excess.Boring ID runout found 0.12 mm.O
 
6. Inspection Method Analysis (Current)
Inspection Method Instrument
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size Sampling
7. Root Cause Analysis (Occurance)
Why 1 Thread runout wrt groove diameter is more
Why 2 line mark on boring face.
Why 3 insert corner break.
Why 4 boring time job not clamp properly.
Why 5 chuck jaw was break due to minor accident on the machine but this time jaw condition not inspect.
Root Cause (Occurance) Chuck jaw was break that why job not clamp properly and insert corner is break.
 
Root Cause Analysis (Outflow)
Why 1 Thread runout wrt groove diameter is more.
Why 2 Excess runout piece not detect at final inspection side.
Why 3 due to inspect runout at final inspection sampling basis.
Why 4
Why 5
Root Cause (Outflow) Runout inspection frequency is low at final inspection.
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OutflowRunout sampling inspection frequency increase at final inspection time.Gopinath Gore17/06/202417/06/2024Completed
OccuranceStart inspection at time boring done and also start daily chuck jaw condition.Gaurav Mhaske11/05/202411/05/2024Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details start inspection at time of boring setup approval.
Inspection Method Instrument
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size Sampling.
10. Evidance of Countermeasure
Occurance (Before) Thread runout wrt groove diameter inspection not done boring setup approval time.
778_Occurance_Before.xlsx
Occurance (After) Thread runout wrt groove diameter inspection done boring setup approval time and CNC Chuck jaw inspection done.
778_Occurance_After.xlsx
Outflow (Before) Before Sampling plan inspection frequency.
778_Outflow_Before.xlsx
Outflow (After) Revise sampling plan frequency change.
778_Outflow_After.xlsx
 
11. Horizontal Deployment
Horizontal Deployment Required No
Applicable Machine / Model / Plant No
 
12. Document Review
Documents ControlPlan, InspCheckSheet
Specify Other Document NO
 
13. Effectiveness Of Action
Reviewed Quantity 100
Reason for submission OK