QFR No - 8000873486
Defect Details
NC No. 8000873486
NC Date 06/05/2024
NC Submission Date
Part No. F2LG03702B
Part Name SEAT PIPE (K1 UG)
Supplier Name & Code 100648-JOTIBA TECHNOLOGIES PVT.LTD.
ETL Plant 1117-ETL K-228/9 Suspension
Defect Details NOT AS PER SPECIFICATION-THREADING INCOMPLETE
 
1. Problem Description
Defect Description THREADING INCOMPLETE
Detection Stage Inprocess
Problem Severity Function
NG Quantity 1
Is Defect Repeatative? No
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID accjotiba@gmail.com
Plant Head/CEO Email ID sanghavi.rajesh@sanghavigroup.co.in
MD Email ID jotibatech@gmail.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
1050
0
0
1200
2000
4250
Check Qty
1050
0
0
1200
2000
4250
NG Qty
1
0
0
0
0
1
 
Scrap 1
Rework 0
Under Deviation 0
Containment Action
Model wise marking on spacer plate of job stopper.
 
3. Process Flow
Process Flow Description
10.Raw material Inspection ,20.Parting Off 30.Chamfer,40.Weighing,50.Draw Forging,60.Hex Forging,70.Rough Grinding,80.Collar Machining,90.Total length facing and Boring,100.Piercing,110.DF Hole chamfering,120. Compression Hole chamfering, 130.ID Reaming,140.Tapping,150.Finish Grinding,160.Final Inspection,170.ID Cleaning,180.Ultrasonic Cleaning,190.Apply antirust oil,200.Packing and Dispatch.
 
4. Process Details
Process / Operation 140.Tapping
Outsource No
Machine / Cell Tapping
Machine / Cell No. Tapping 01
5. Problem Analysis
Type Possible Cause Fact Verification Jud
ToolTap use excess compare to tap life set that why wear out coating of tap.Set interlock of machine tap life.O
ToolNo model wise marking on spacer plate.Not inspect spacer plate size.O
MachinePM not done on time.PM done on time.O
MaterialInput size of bore diameter undersize.Input size of bore is found ok.O
ManNot inspect spacer plate before assembly of stopper.Operator knows only who to assembly of stopper.X
MethodThere is no cross verification of after setup ok or not okOperator not know how to check setup ok or Not ok.O
 
6. Inspection Method Analysis (Current)
Inspection Method Sp. Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size Sampling
7. Root Cause Analysis (Occurance)
Why 1 Half tapping part produce.
Why 2 While set-up changing time wrong width spacer plate use.
Why 3 Operator not check width of spacer plate during set-up time.
Why 4
Why 5
Root Cause (Occurance) No model wise marking on spacer plate of stopper.
 
Root Cause Analysis (Outflow)
Why 1 Half tapping part not detect at final inspection.
Why 2 Inspect part at final inspection is visually.
Why 3 Available thread plug gauge for inspection thread but length GO thread gauge is less.
Why 4 No special gauge for inspection half tapping job.
Why 5
Root Cause (Outflow) No special gauge for inspection of half tapping job.
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceAfter setup change cross check setting is ok or not ok use setting block.Gopinath Gore06/06/202403/06/2024Completed
OccuranceModel wise mark on spacer plate.Gopinath Gore08/05/202408/05/2024Completed
OutflowAdd special gauge for inspection with 100% identification mark on job.Gopinath Gore11/05/202411/05/2024Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details 100% inspection with identification mark on job and add special gauge for inspection of tapping.
Inspection Method Sp. Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size sampling
10. Evidance of Countermeasure
Occurance (Before) No identification mark on spacer plate of stopper.
779_Occurance_Before.xlsx
Occurance (After) Identification mark on spacer plate of stopper.
779_Occurance_After.xlsx
Outflow (Before) Inspect part as per sampling plan and visually.
779_Outflow_Before.xlsx
Outflow (After) 100% Visually inspection with identification mark and use special gauge for checking.
779_Outflow_After.xlsx
 
11. Horizontal Deployment
Horizontal Deployment Required No
Applicable Machine / Model / Plant NA
 
12. Document Review
Documents ControlPlan
Specify Other Document Special Gauge
 
13. Effectiveness Of Action
Reviewed Quantity 150
Reason for submission Ok