QFR No - 8000873488
Defect Details
NC No. 8000873488
NC Date 06/05/2024
NC Submission Date
Part No. F2LG07702B
Part Name SEAT PIPE - J1C2 FF
Supplier Name & Code 100539-N P ENTERPRISES
ETL Plant 1117-ETL K-228/9 Suspension
Defect Details NOT AS PER SPECIFICATION-TOTAL LENGTH UNDERSIZE
 
1. Problem Description
Defect Description TOTAL LENGTH UNDERSIZE
Detection Stage Inprocess
Problem Severity Fitment
NG Quantity 4
Is Defect Repeatative? Yes
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID quality@npcindustries.in
Plant Head/CEO Email ID anand@npcindustries.in
MD Email ID ajay@npcindustries.in
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
960
7120
1245
0
0
9325
Check Qty
960
0
1245
0
0
2205
NG Qty
5
0
0
0
0
5
 
Scrap 5
Rework 0
Under Deviation 0
Containment Action
Segregation Done At ETL and NP end.
 
3. Process Flow
Process Flow Description
Process Flow Description 1.0 Raw Material 2.0 Cutting 3.0 Drawing 4.0 Head Formation 5.0 Rough Grinding 6.0 Punching 7.0 CNC Head Turning 8.0 CNC Boring & Facing 9.0 Tapping 10.0 Chamfering 11.0 ID Deburring 12.0 Finish Grinding 13.0 Final Inspection 14.0 Cleaning 15.0 Oiling 16.0 Packing &Dispatch.
 
4. Process Details
Process / Operation CNC Boring
Outsource No
Machine / Cell CNC Boring & Chamfering
Machine / Cell No. CNC SP1
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MethodStopper design not adequateStopper design observed to be adequateO
MethodHead Stopper looseHead Stopper found to be tightO
ManNegligence of quality inspector at in processQuality inspector found to be non negligent .O
ManOperator unawareOperator found to be aware about the processO
MethodOperator located part incorrectly during Facing operationIt was verified and observed that Operator is locating part incorrectly. This is resulting in extraX
MethodNG part skipped at Final inspectionIt was verified and observed that parts skipped during sampling at final inspectionX
MethodBurr on Stopper pinNo burr observed on Stopper pinO
MaterialMaterial Hardness moreReceiving inspection report verified . Material hardness found to be within limits. 35 – 55 HRBO
MachineWrong Program runAfter verification we found correct Program run as per std.O
 
6. Inspection Method Analysis (Current)
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size As per std
7. Root Cause Analysis (Occurance)
Why 1 Total length undersize
Why 2 Facing operation done incorrectly
Why 3 Extra Facing done
Why 4 Operator located part incorrectly
Why 5
Root Cause (Occurance) Operator located part incorrectly
 
Root Cause Analysis (Outflow)
Why 1 Total length undersize
Why 2 Could not be detected at Final Inspection
Why 3 Skipped in Sampling inspection
Why 4
Why 5
Root Cause (Outflow) Skipped in Sampling inspection
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceQuality alert to be displayed at CNC stationMr. Prince07/05/202406/05/2024Completed
OccuranceTraining to be provided to all CNC operatorsMr. MohinderPal10/05/202408/05/2024Completed
OccuranceMin level 3 operator will be allowed to operate CNC Facing MachineMr. Harwinder08/05/202407/05/2024Completed
Outflow100% inspection with Length Snap Gauge to be done before dispatchMr. Vinay07/05/202406/05/2024Completed
OutflowLength Snap Gauge to be provided at Godown for Sampling InspectionMr. Mohinder Pal11/05/202409/05/2024Completed
OccuranceHome position of insert to be changed from 22mm to 2.5mmMr. Harwinder11/05/202410/05/2024Completed
OutflowQuality alert to be displayed at final inspection stationMr. Princ07/05/202406/05/2024Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details 100 % inspection to be start for total length
Inspection Method Sp. Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
10. Evidance of Countermeasure
Occurance (Before) Home position of insert was 22mm
781_Occurance_Before.png
Occurance (After) Home position of insert to be changed from 22mm to 2.5mm Training to be provided to all CNC operators
781_Occurance_After.png
Outflow (Before) Sampling inspection was being conducted for length
781_Outflow_Before.png
Outflow (After) 100 % Inspection to be start with length gauge.
781_Outflow_After.jpg
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant similar model
 
12. Document Review
Documents ControlPlan, PFMEA, WISOP, AuditCheckSheet, InspCheckSheet
Specify Other Document NO
 
13. Effectiveness Of Action
Reviewed Quantity 180
Reason for submission OK