QFR No - 8000873531
Defect Details
NC No. | 8000873531 |
NC Date | 06/05/2024 |
NC Submission Date | |
Part No. | F2LG07102B |
Part Name | SEAT PIPE - J1D |
Supplier Name & Code | 101263-SINGLA PRECISION SCREWS |
ETL Plant | 1117-ETL K-228/9 Suspension |
Defect Details | NOT AS PER SPECIFICATION-TOTAL LENGTH UNDERSIZE |
1. Problem Description
Defect Description | TOTAL LENGTH UNDERSIZE |
Detection Stage | Inprocess |
Problem Severity | Fitment |
NG Quantity | 1 |
Is Defect Repeatative? | No |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | quality@singlaprecision.com |
Plant Head/CEO Email ID | quality@singlaprecision.com |
MD Email ID | aditya@singlaprecision.com |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
600
|
0
|
0
|
0
|
0
|
600
|
Check Qty |
600
|
0
|
0
|
0
|
0
|
600
|
NG Qty |
1
|
0
|
0
|
0
|
0
|
1
|
Scrap | 1 |
Rework | 0 |
Under Deviation | 0 |
Containment Action |
---|
STOCK CHECK 100% AT OUR END |
3. Process Flow
Process Flow Description |
---|
1-RM 2- FORGING 3-PUNCHING -IST 4-ROUGH CLG 5-CNC-IST 6-CNC-II 7-PUNCHING -II 8-I.D CHIP REMOVE 9-REAMING IST 10-REAMING-IIND 11-TAPPING 12-FINAL GRINDING 13-ALKLINE WASHING 14- FINAL INSPECTION 15 - PACKING |
4. Process Details
Process / Operation | CNC -2ND OPERATION |
Outsource | No |
Machine / Cell | CNC-MACHINE |
Machine / Cell No. | CNC -5 |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Material | RM GRADE AND SIZE NOT OK | VALIDATED AND FOUND OK | O |
Man | UNAWARENESS OF OPERATOR | VALIDATION AND FOUND MACHINE OPERATOR ABOUT TOOL LIFE FRQ NOT AWARENESS | X |
Tool | TOOL MAY BE WEAR | VALIDATE AND FOUND WEAROUT | X |
Method | INSPECTION METHOD NOT EFFECTIVE | VALIDATION AND FOUND TOTAL LENTH CHECKING INSTRUMENT NOT FOUND IN MACHINE | X |
Machine | MACHINE PM NOT EFFECTIVE | MACHINE AIR GUN NOT WORKING CHIPS NOT CLEAN ON COLLECT | X |
6. Inspection Method Analysis (Current)
Inspection Method | Instrument |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | NO |
7. Root Cause Analysis (Occurance)
Why 1 | TOTAL LENGTH UNDERSIZE |
Why 2 | Due to the presence of a chip in the collect chips the part was not properly set on place |
Why 3 | Operator Air gun not use |
Why 4 | OPERATOR WI NOT ADD PART PER CYCLE AIR GUN USE IN COLLET |
Why 5 | OPERATOR NOT AWRE THIS TYPE OF PROBLEM |
Root Cause (Occurance) | OPERATOR WI NOT ADD PART PER CYCLE AIR GUN USE IN COLLET |
Root Cause Analysis (Outflow)
Why 1 | TOTAL LENGTH UNDERSIZE |
Why 2 | INSPECTION PLAN WAS NOT EFFECTIVE |
Why 3 | AS PER SAMPLING PLAN PART CHECKING IN FINAL INSPECTION |
Why 4 | LENGTH DIAL GAUGE NOT AVAILABLE IN MACHINE AND FINAL INSPECTION |
Why 5 | NG PART SKIPPED FROM INSPECTION AND MACHINE |
Root Cause (Outflow) | LENGTH DIAL GAUGE NOT AVAILABLE IN MACHINE AND FINAL INSPECTION |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Outflow | DIAL LENGTH GAUGE PROVIDE TO MACHINE AND FINAL INSPECTION | MR GANESH MAURYA | 09/05/2024 | 09/05/2024 | Completed |
Occurance | OPERATOR WI NOT ADD PART PER CYCLE AIR GUN USE IN COLLET | ASHISH SINGH | 09/05/2024 | 09/05/2024 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | Yes |
Change Details | DIAL LENGTH GAUGE PROVIDE TO MACHINE AND FINAL INSPECTION |
Inspection Method | Sp. Gauge |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | Sampling |
Sampling | No |
Sample Size | 50/1200 |
10. Evidance of Countermeasure
Occurance (Before) |
OPERATOR WI NOT ADD PART PER CYCLE AIR GUN USE IN COLLET 784_Occurance_Before.xlsx |
Occurance (After) |
OPERATOR WI ADD PART PER CYCLE AIR GUN USE IN COLLET 784_Occurance_After.xlsx |
Outflow (Before) |
Gauge not implements 784_Outflow_Before.xlsx |
Outflow (After) |
100% gauge implements 784_Outflow_After.xlsx |
11. Horizontal Deployment
Horizontal Deployment Required | Yes |
Applicable Machine / Model / Plant | CNC -05 PLANT NO -177 |
12. Document Review
Documents | PokayokeCheckSheet, PFMEA |
Specify Other Document | NO |
13. Effectiveness Of Action
Reviewed Quantity | 100 |
Reason for submission | Due to the presence of a chip in the collect chips the part was not properly set on place - Use pokayoke or interlocking like- 1. Seat check pokayoke required to ensure perfect seating/ resting of part 2. Provision of coolant flow with 5 bar pressure interlock with machine cycle. 3. Share pokayoke details |