QFR No - 8000873536
Defect Details
NC No. | 8000873536 |
NC Date | 06/05/2024 |
NC Submission Date | |
Part No. | F2DZ07203B |
Part Name | FORK BOLT (K-9207) Ni+Cr Plated |
Supplier Name & Code | 100539-N P ENTERPRISES |
ETL Plant | 1117-ETL K-228/9 Suspension |
Defect Details | NOT AS PER SPECIFICATION-PLATING MISSING |
1. Problem Description
Defect Description | PLATING MISSING |
Detection Stage | Inprocess |
Problem Severity | Aesthetic |
NG Quantity | 2 |
Is Defect Repeatative? | Yes |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | quality@npcindustries.in |
Plant Head/CEO Email ID | anand@npcindustries.in |
MD Email ID | ajay@npcindustries.in |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
1500
|
50000
|
0
|
0
|
0
|
51500
|
Check Qty |
1500
|
50000
|
0
|
0
|
0
|
51500
|
NG Qty |
2
|
0
|
0
|
0
|
0
|
2
|
Scrap | 2 |
Rework | 0 |
Under Deviation | 0 |
Containment Action |
---|
1.Raw Material 2. Blanking 3. Hex Punching 4. Flattening 5. CNC Turning, Chamfering & threading 6. Buffing 7. Plating 8.Final Inspection. |
3. Process Flow
Process Flow Description |
---|
10 - Raw Material 20 - Cutting and Forging(1st) 30-Forging(2nd) 40-Annealing 50-Phosphating 60 - Forging(3rd) I.D 70-Forging(4th) Hex 80 - CNC(1st) 90 - CNC(2nd) 100 - CNC(3rd) 110 - CNC drilling and Chamfering 120 - Final inspection 130 - Packing & Dispatch 140 - Buffing-1st 150 - Buffing 2nd 160 - Plating |
4. Process Details
Process / Operation | Plating |
Outsource | Yes |
Machine / Cell | Plating plant |
Machine / Cell No. | NA |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Material | Plating chemicals composition was not as per spec. | After verification we found OK | O |
Man | Untrained Operator | After verification we found operator was aware about process and responsibilities | O |
Method | Plating time duration less | After verification we observed plating time duration as per std. | O |
Method | PC position holding method NG | During verification we found Jig holder was damage | X |
Method | Skipped during final inspection | after verification we found part was skipped at final inspection. | X |
6. Inspection Method Analysis (Current)
Inspection Method | Other |
Other Inspection Method | visual |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100% |
7. Root Cause Analysis (Occurance)
Why 1 | The bolt was not correctly positioned during the plating process. |
Why 2 | The jig point, which is supposed to hold the bolt securely, was not clean. |
Why 3 | The jig cleaning process was either inadequate or not performed regularly. |
Why 4 | There was no clear protocol or schedule for cleaning the jig points. |
Why 5 | WI did not include guidelines for the regular cleaning of jig points. |
Root Cause (Occurance) | WI did not include guidelines for the regular cleaning of jig points. |
Root Cause Analysis (Outflow)
Why 1 | Plating NG in fork bolt. |
Why 2 | Defected part could not detect |
Why 3 | The part was skipped at final Q-gate. |
Why 4 | NG and OK pc was put at the same color of bin. |
Why 5 | |
Root Cause (Outflow) | NG and OK pc was put at the same color of bin. |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Outflow | Locked red bin implement at the Final Q gate | Nikhil Jain | 11/05/2024 | 11/05/2024 | Completed |
Outflow | Q-alert to be displayed at final Q gate | Mr. Deepak | 08/05/2024 | 07/05/2024 | Completed |
Occurance | Regular cleaning of jig points to be added in WI | Nikhil Jain | 10/05/2024 | 09/05/2024 | Completed |
Outflow | Blue bin used for without checked material and Green bin used for Checked material. | Nikhil Jain | 15/05/2024 | 11/05/2024 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | Yes |
Change Details | Same color of bin to be replaced with different color for different purpose. |
Inspection Method | Other |
Other Inspection Method | Visual |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100% |
10. Evidance of Countermeasure
Occurance (Before) |
WI did not include guidelines for the regular cleaning of jig points. 788_Occurance_Before.jpg |
Occurance (After) |
updated wi to be updated 788_Occurance_After.jpg |
Outflow (Before) |
NG and OK pc was put at the same color of bin. 788_Outflow_Before.jpeg |
Outflow (After) |
NG pcs put in orange bin and OK pc was put in Blue bin and red bin implement 788_Outflow_After.pdf |
11. Horizontal Deployment
Horizontal Deployment Required | Yes |
Applicable Machine / Model / Plant | All Similar parts |
12. Document Review
Documents | PMCheckSheet, PFMEA, WISOP |
Specify Other Document | Na |
13. Effectiveness Of Action
Reviewed Quantity | 50 |
Reason for submission | ok |