QFR No - 8000873540
Defect Details
NC No. | 8000873540 |
NC Date | 06/05/2024 |
NC Submission Date | |
Part No. | 550PC09107 |
Part Name | UNDER BKT M/C (CT100) |
Supplier Name & Code | 101222-SANGKAJ ENGINEERING PVT LTD- U |
ETL Plant | 1117-ETL K-228/9 Suspension |
Defect Details | NOT AS PER SPECIFICATION-ID UNDERSIZE |
1. Problem Description
Defect Description | ID UNDERSIZE |
Detection Stage | Receipt |
Problem Severity | Fitment |
NG Quantity | 6 |
Is Defect Repeatative? | Yes |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | irfan@sangkaj.com |
Plant Head/CEO Email ID | steel@sangkaj.com |
MD Email ID | anirudh.2007@hotmail.com |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
320
|
0
|
0
|
0
|
0
|
320
|
Check Qty |
320
|
0
|
0
|
0
|
0
|
320
|
NG Qty |
6
|
0
|
0
|
0
|
0
|
6
|
Scrap | 6 |
Rework | 0 |
Under Deviation | 0 |
Containment Action |
---|
checked all ETL end and pipe line material |
3. Process Flow
Process Flow Description |
---|
forging inward-pre drilling- ruff boring-5.1 drill-boss drilling lug milling- slitting-counter drilling-M6 tapping- M8 tapping- final inspection. |
4. Process Details
Process / Operation | ruff boring |
Outsource | No |
Machine / Cell | under bracket semi finish line |
Machine / Cell No. | ruff boring |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Man | Inspector did not follow the SOP for inspection | Final inspection report is evident | O |
Material | Burr generated at rough boring stage | Verified burr not found | O |
Method | master setting ring not ok | verified master setting ring having ovality and tapper | X |
Tool | Tool life monitoring not effective | Tool life monitoring found not as per plan | X |
6. Inspection Method Analysis (Current)
Inspection Method | Gauge |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100% |
7. Root Cause Analysis (Occurance)
Why 1 | 28 mm Center bore ID undersize produced |
Why 2 | due to tool wear tool size gets undersize |
Why 3 | tool not changed at defined life |
Why 4 | No any alarm/information to operator after life over |
Why 5 | |
Root Cause (Occurance) | No any alarm/information to operator after life over |
Root Cause Analysis (Outflow)
Why 1 | 28 mm Center bore ID undersize found at customer end. |
Why 2 | 28 mm Center bore ID undersize not detected at final inspection. |
Why 3 | Air gauge master ring found ovality and tapper before calibration due date. |
Why 4 | |
Why 5 | |
Root Cause (Outflow) | Air gauge master ring found ovality and tapper before calibration due date. |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Occurance | Interlock mechanism for tool life on boring SPM. | Mr.Sayyed | 10/06/2024 | 11/06/2024 | Completed |
Outflow | Revise calibration frequency from 1 year to 6 Month | Mr.Sayyed | 16/05/2024 | 15/05/2024 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | No |
Change Details | Revise calibration frequency from 1 year to 6 Month |
Inspection Method | Gauge |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100% |
10. Evidance of Countermeasure
Occurance (Before) |
air gauge master setting ring found ovality and tapper 791_Occurance_Before.jpg |
Occurance (After) |
ok master setting ring provided 791_Occurance_After.jpg |
Outflow (Before) |
Manual tool life monitoring 791_Outflow_Before.jpg |
Outflow (After) |
Part counter with buzzer alarm implemented 791_Outflow_After.jpg |
11. Horizontal Deployment
Horizontal Deployment Required | No |
Applicable Machine / Model / Plant | SPM ruff boring Machine |
12. Document Review
Documents | WISOP |
Specify Other Document | work instruction |
13. Effectiveness Of Action
Reviewed Quantity | 50 |
Reason for submission | ok |