QFR No - 8000873540
Defect Details
NC No. 8000873540
NC Date 06/05/2024
NC Submission Date
Part No. 550PC09107
Part Name UNDER BKT M/C (CT100)
Supplier Name & Code 101222-SANGKAJ ENGINEERING PVT LTD- U
ETL Plant 1117-ETL K-228/9 Suspension
Defect Details NOT AS PER SPECIFICATION-ID UNDERSIZE
 
1. Problem Description
Defect Description ID UNDERSIZE
Detection Stage Receipt
Problem Severity Fitment
NG Quantity 6
Is Defect Repeatative? Yes
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID irfan@sangkaj.com
Plant Head/CEO Email ID steel@sangkaj.com
MD Email ID anirudh.2007@hotmail.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
320
0
0
0
0
320
Check Qty
320
0
0
0
0
320
NG Qty
6
0
0
0
0
6
 
Scrap 6
Rework 0
Under Deviation 0
Containment Action
checked all ETL end and pipe line material
 
3. Process Flow
Process Flow Description
forging inward-pre drilling- ruff boring-5.1 drill-boss drilling lug milling- slitting-counter drilling-M6 tapping- M8 tapping- final inspection.
 
4. Process Details
Process / Operation ruff boring
Outsource No
Machine / Cell under bracket semi finish line
Machine / Cell No. ruff boring
5. Problem Analysis
Type Possible Cause Fact Verification Jud
ManInspector did not follow the SOP for inspectionFinal inspection report is evidentO
MaterialBurr generated at rough boring stageVerified burr not foundO
Methodmaster setting ring not okverified master setting ring having ovality and tapperX
ToolTool life monitoring not effectiveTool life monitoring found not as per planX
 
6. Inspection Method Analysis (Current)
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
7. Root Cause Analysis (Occurance)
Why 1 28 mm Center bore ID undersize produced
Why 2 due to tool wear tool size gets undersize
Why 3 tool not changed at defined life
Why 4 No any alarm/information to operator after life over
Why 5
Root Cause (Occurance) No any alarm/information to operator after life over
 
Root Cause Analysis (Outflow)
Why 1 28 mm Center bore ID undersize found at customer end.
Why 2 28 mm Center bore ID undersize not detected at final inspection.
Why 3 Air gauge master ring found ovality and tapper before calibration due date.
Why 4
Why 5
Root Cause (Outflow) Air gauge master ring found ovality and tapper before calibration due date.
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceInterlock mechanism for tool life on boring SPM.Mr.Sayyed10/06/202411/06/2024Completed
OutflowRevise calibration frequency from 1 year to 6 MonthMr.Sayyed16/05/202415/05/2024Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System No
Change Details Revise calibration frequency from 1 year to 6 Month
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
10. Evidance of Countermeasure
Occurance (Before) air gauge master setting ring found ovality and tapper
791_Occurance_Before.jpg
Occurance (After) ok master setting ring provided
791_Occurance_After.jpg
Outflow (Before) Manual tool life monitoring
791_Outflow_Before.jpg
Outflow (After) Part counter with buzzer alarm implemented
791_Outflow_After.jpg
 
11. Horizontal Deployment
Horizontal Deployment Required No
Applicable Machine / Model / Plant SPM ruff boring Machine
 
12. Document Review
Documents WISOP
Specify Other Document work instruction
 
13. Effectiveness Of Action
Reviewed Quantity 50
Reason for submission ok