QFR No - 8000874414
Defect Details
NC No. | 8000874414 |
NC Date | 15/05/2024 |
NC Submission Date | |
Part No. | 080FA04033 |
Part Name | FORK PIPE MACHINED |
Supplier Name & Code | 101222-SANGKAJ ENGINEERING PVT LTD- U |
ETL Plant | 1117-ETL K-228/9 Suspension |
Defect Details | NOT AS PER SPECIFICATION-THREADING NG |
1. Problem Description
Defect Description | THREADING NG |
Detection Stage | Inprocess |
Problem Severity | Safety |
NG Quantity | 14 |
Is Defect Repeatative? | Yes |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | aslam@sangkaj.com |
Plant Head/CEO Email ID | steel@sangkaj.com |
MD Email ID | anirudh.2007@hotmail.com |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
800
|
0
|
0
|
0
|
0
|
800
|
Check Qty |
800
|
0
|
0
|
0
|
0
|
800
|
NG Qty |
14
|
0
|
0
|
0
|
0
|
14
|
Scrap | 14 |
Rework | 0 |
Under Deviation | 0 |
Containment Action |
---|
Segregation done at ETL end. |
3. Process Flow
Process Flow Description |
---|
Tube RM inward - Induction hardening - CNC 1st - CNC 2nd - Drilling - Visual inspection - Bundling - Dispatch |
4. Process Details
Process / Operation | CNC-1st |
Outsource | No |
Machine / Cell | CNC-05 |
Machine / Cell No. | CNC-05 |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Material | ID of tube is more than TRD ID | Inward inspection done | X |
Method | Tool position disturbed | Every thing is controlled by program | X |
Man | operator did not follow the measuring procedure | Hourly inspection report is updated | X |
Tool | insert worn-out. | Micro program is available. | O |
Machine | Turret bearing worn out | PM done on time | X |
6. Inspection Method Analysis (Current)
Inspection Method | Gauge |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | Sampling |
Sampling | No |
Sample Size | 10:500 |
7. Root Cause Analysis (Occurance)
Why 1 | Fork pipe machined -THREADING NG (Go gauge not qualifying) |
Why 2 | Insert worn out. |
Why 3 | insert worn out before defined life in micro program |
Why 4 | Tool life defined is not ok. |
Why 5 | Validation for tool life is in adequate. |
Root Cause (Occurance) | Validation for tool life is in adequate. |
Root Cause Analysis (Outflow)
Why 1 | Fork pipe machined -THREADING NG (Go gauge not qualifying) |
Why 2 | Inspection done as per defined frequency ,i.e 10:500. |
Why 3 | Frequency for inspection is less in CP. |
Why 4 | CP for final inspection is inadequate. |
Why 5 | |
Root Cause (Outflow) | CP for final inspection is inadequate. |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Occurance | Re-validation to be done for tool life. | Mr. Krushna Phuke | 30/05/2024 | 31/05/2024 | Completed |
Outflow | CP to be updated for inspection frequency. | Mr. Aslam Shaikh | 30/05/2024 | 31/05/2024 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | Yes |
Change Details | Frequency of inspection changed from 10:500 to 50:500. |
Inspection Method | Gauge |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | Sampling |
Sampling | No |
Sample Size | 50:500 |
10. Evidance of Countermeasure
Occurance (Before) |
CNC program before - tool life defined as per previous experience only 813_Occurance_Before.pdf |
Occurance (After) |
CNC program after- Tool life defined as per validation report. 813_Occurance_After.pdf |
Outflow (Before) |
CP - Before ( inspection frequency 10:500 ) 813_Outflow_Before.pdf |
Outflow (After) |
CP - After ( inspection frequency increased 10:500 to 50:500 813_Outflow_After.pdf |
11. Horizontal Deployment
Horizontal Deployment Required | Yes |
Applicable Machine / Model / Plant | All similar models. |
12. Document Review
Documents | ControlPlan |
Specify Other Document | No |
13. Effectiveness Of Action
Reviewed Quantity | 100 |
Reason for submission | Accepted |