QFR No - 8000874414
Defect Details
NC No. 8000874414
NC Date 15/05/2024
NC Submission Date
Part No. 080FA04033
Part Name FORK PIPE MACHINED
Supplier Name & Code 101222-SANGKAJ ENGINEERING PVT LTD- U
ETL Plant 1117-ETL K-228/9 Suspension
Defect Details NOT AS PER SPECIFICATION-THREADING NG
 
1. Problem Description
Defect Description THREADING NG
Detection Stage Inprocess
Problem Severity Safety
NG Quantity 14
Is Defect Repeatative? Yes
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID aslam@sangkaj.com
Plant Head/CEO Email ID steel@sangkaj.com
MD Email ID anirudh.2007@hotmail.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
800
0
0
0
0
800
Check Qty
800
0
0
0
0
800
NG Qty
14
0
0
0
0
14
 
Scrap 14
Rework 0
Under Deviation 0
Containment Action
Segregation done at ETL end.
 
3. Process Flow
Process Flow Description
Tube RM inward - Induction hardening - CNC 1st - CNC 2nd - Drilling - Visual inspection - Bundling - Dispatch
 
4. Process Details
Process / Operation CNC-1st
Outsource No
Machine / Cell CNC-05
Machine / Cell No. CNC-05
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MaterialID of tube is more than TRD IDInward inspection doneX
MethodTool position disturbedEvery thing is controlled by programX
Manoperator did not follow the measuring procedureHourly inspection report is updatedX
Toolinsert worn-out.Micro program is available.O
MachineTurret bearing worn outPM done on timeX
 
6. Inspection Method Analysis (Current)
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size 10:500
7. Root Cause Analysis (Occurance)
Why 1 Fork pipe machined -THREADING NG (Go gauge not qualifying)
Why 2 Insert worn out.
Why 3 insert worn out before defined life in micro program
Why 4 Tool life defined is not ok.
Why 5 Validation for tool life is in adequate.
Root Cause (Occurance) Validation for tool life is in adequate.
 
Root Cause Analysis (Outflow)
Why 1 Fork pipe machined -THREADING NG (Go gauge not qualifying)
Why 2 Inspection done as per defined frequency ,i.e 10:500.
Why 3 Frequency for inspection is less in CP.
Why 4 CP for final inspection is inadequate.
Why 5
Root Cause (Outflow) CP for final inspection is inadequate.
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceRe-validation to be done for tool life.Mr. Krushna Phuke30/05/202431/05/2024Completed
OutflowCP to be updated for inspection frequency.Mr. Aslam Shaikh30/05/202431/05/2024Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details Frequency of inspection changed from 10:500 to 50:500.
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size 50:500
10. Evidance of Countermeasure
Occurance (Before) CNC program before - tool life defined as per previous experience only
813_Occurance_Before.pdf
Occurance (After) CNC program after- Tool life defined as per validation report.
813_Occurance_After.pdf
Outflow (Before) CP - Before ( inspection frequency 10:500 )
813_Outflow_Before.pdf
Outflow (After) CP - After ( inspection frequency increased 10:500 to 50:500
813_Outflow_After.pdf
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant All similar models.
 
12. Document Review
Documents ControlPlan
Specify Other Document No
 
13. Effectiveness Of Action
Reviewed Quantity 100
Reason for submission Accepted