QFR No - 8000874503
Defect Details
NC No. | 8000874503 |
NC Date | 16/05/2024 |
NC Submission Date | |
Part No. | F2PH01302B |
Part Name | VALVE RETAINER (K-1015) |
Supplier Name & Code | 101255-MAHAVIR INDUSTRIES |
ETL Plant | 1117-ETL K-228/9 Suspension |
Defect Details | NOT AS PER SPECIFICATION-ID UNDERSIZE (BURR REVOLVED) |
1. Problem Description
Defect Description | ID undersize |
Detection Stage | Inprocess |
Problem Severity | Fitment |
NG Quantity | 10 |
Is Defect Repeatative? | No |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | quality@mahavirind.co.in |
Plant Head/CEO Email ID | planthead@mahavirind.co.in |
MD Email ID |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
1200
|
0
|
0
|
1500
|
0
|
2700
|
Check Qty |
1200
|
0
|
0
|
1500
|
0
|
2700
|
NG Qty |
10
|
0
|
0
|
3
|
0
|
13
|
Scrap | 10 |
Rework | 3 |
Under Deviation | 0 |
Containment Action |
---|
All Suspected material Segregation at Customer End |
3. Process Flow
Process Flow Description |
---|
RM Inward at MI K-11- Store at Janki Engineering - Parting on Traub machine - Chamfer on Drill machine - Inward Inspection at k-11-Counter Boring on CNC Machine - Plating Green Passivation - Final Inspection - Dispatch |
4. Process Details
Process / Operation | Counter Boring on CNC |
Outsource | No |
Machine / Cell | CNC Cell |
Machine / Cell No. | CNC-02 |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Man | Unskilled operator | As per skilled matrix chart skilled operator | O |
Tool | Wrong Insert Use For Facing Operation | Correct Insert TNMGG04 use for Facing operation | O |
Method | Wrong Inspection Instruments | Plain PPG use Instead of step gauge on CNC Machien | X |
Material | Hard Material | Material Hardness Found 78-82 HRB | O |
Machine | During Counter facing Operation Facing tool over feed | During Counter Facing operation Feed obs. 0.15mm/Rev. Instead of 0.12mm/Rev. | X |
6. Inspection Method Analysis (Current)
Inspection Method | Sp. Gauge |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | Sampling |
Sampling | No |
Sample Size | 5Nos/Hr |
7. Root Cause Analysis (Occurance)
Why 1 | Not as per specification -ID Undersize Burr fold At ID |
Why 2 | Feed Over During Valve Retainer Job Change Over. |
Why 3 | During Job Change Over Valve Retainer facing tool Process Parameters Not Correction in program on CNC machine. |
Why 4 | During Counter Operation Process Facing Tool Over Feed of Facing Tool on CNC Machine. |
Why 5 | |
Root Cause (Occurance) | During Counter Operation Process Facing Tool Over Feed of Facing Tool on CNC Machine. |
Root Cause Analysis (Outflow)
Why 1 | Not as per specification -ID Undersize Burr fold At ID |
Why 2 | Counter ID Fold Burr not detect on final inspection |
Why 3 | ID Inspection By Plain PPG |
Why 4 | |
Why 5 | |
Root Cause (Outflow) | ID Inspection By Plain PPG |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Occurance | Counter Facing tool process parameter Feed Reduce -0.12mm/rev. Instead of 0.15mm/rev | Production Head / Quality Head | 20/05/2024 | 21/05/2024 | Completed |
Outflow | New Step Gauge Provide on CNC Machine and Final Inspection Stage | Quality Head | 20/05/2024 | 30/05/2024 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | Yes |
Change Details | Step Gauge Provide On CNC Machine |
Inspection Method | Sp. Gauge |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100% |
10. Evidance of Countermeasure
Occurance (Before) |
During Counter Operation Process Facing Tool Over Feed of Facing Tool on CNC Machine. 808_Occurance_Before.jpg |
Occurance (After) |
Counter Facing tool process parameter Feed Reduce -0.12mm/rev. Instead of 0.15mm/rev 808_Occurance_After.jpg |
Outflow (Before) |
Required Special Gauge Not Available For Both Counter ID at time Inspection. 808_Outflow_Before.jpg |
Outflow (After) |
New Step Gauge Provide on CNC Machine and Final Inspection Stage 808_Outflow_After.jpg |
11. Horizontal Deployment
Horizontal Deployment Required | Yes |
Applicable Machine / Model / Plant | All Valve Retainer Family |
12. Document Review
Documents | ControlPlan, PFMEA |
Specify Other Document | no |
13. Effectiveness Of Action
Reviewed Quantity | 50 |
Reason for submission | OK |