QFR No - 8000874507
Defect Details
NC No. 8000874507
NC Date 16/05/2024
NC Submission Date
Part No. F2LG07102B
Part Name SEAT PIPE - J1D
Supplier Name & Code 100539-N P ENTERPRISES
ETL Plant 1117-ETL K-228/9 Suspension
Defect Details NOT AS PER SPECIFICATION-CRACK - MATERIAL DEFECT
 
1. Problem Description
Defect Description CRACK - MATERIAL DEFECT
Detection Stage Receipt
Problem Severity Safety
NG Quantity 1
Is Defect Repeatative? No
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID quality@npcindustries.in
Plant Head/CEO Email ID anand@npcindustries.in
MD Email ID ajay@npcindustries.in
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
960
20000
0
0
0
20960
Check Qty
960
20000
0
0
0
20960
NG Qty
1
0
0
0
0
1
 
Scrap 1
Rework 0
Under Deviation 0
Containment Action
Segregated all material at the customer end and NP end.
 
3. Process Flow
Process Flow Description
Process Flow Description 1.0 Raw Material 2.0 Cutting 3.0 Drawing 4.0 Head Formation 5.0 Rough Grinding 6.0 Punching 7.0 CNC Head Turning 8.0 CNC Boring & Facing 9.0 Tapping 10.0 Chamfering 11.0 ID Deburring 12.0 Finish Grinding 13.0 Final Inspection 14.0 Cleaning 15.0 Oiling 16.0 Packing &Dispatch.
 
4. Process Details
Process / Operation Raw material
Outsource Yes
Machine / Cell --
Machine / Cell No. --
5. Problem Analysis
Type Possible Cause Fact Verification Jud
Methodsetting part mixed with ok materialDuring verification we found possibility of setting part mixingX
Methodpart was skipped at final Q gate (NPC)Part was skipped during visual inspectionX
MaterialDesignated Grade not useMaterial Observed as per specificationO
MethodProcess Parameters NGAfter verification we found OKO
MethodPreventive MaintenancePreventive maintenance carried out at defined intervalO
ManUn skilled OperatorChecked & Observed that skilled operator was running the line.O
 
6. Inspection Method Analysis (Current)
Inspection Method Other
Other Inspection Method Visual
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
7. Root Cause Analysis (Occurance)
Why 1 one pc head crack found at customer end
Why 2 NG crack setting parts got mixed with ok material
Why 3 NG part kept in open bin
Why 4 Locked bin not available at Draw
Why 5
Root Cause (Occurance) Locked bin not available at Draw
 
Root Cause Analysis (Outflow)
Why 1 Part was skipped at final inspection.
Why 2 Crack was not visible during inspection.
Why 3 Crack might be microscopic and not detectable by naked eye.
Why 4 Inspector may have lacked sufficient training to detect micro-cracks.
Why 5
Root Cause (Outflow) The inspector may have lacked sufficient training to detect micro-cracks.
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OutflowQ -Alert to be displayed at the final Q-gateMr. Princ17/05/202416/05/2024Completed
OutflowMicro crack detection regarding training to be given to NPC final inspection inspectors.Mr. Gurpreet singh20/05/202417/05/2024Completed
OccuranceOpen red bin to be replaced with locked red bin in forging areaMr. Narinder20/05/202418/05/2024Completed
OccuranceTraining to be given to all setters and operators for setting process regarding.Mr. Kulwant21/05/202418/05/2024Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details 100% Visual Inspection
Inspection Method Other
Other Inspection Method Visual & testing met
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
10. Evidance of Countermeasure
Occurance (Before) Open Red bin used
810_Occurance_Before.jpeg
Occurance (After) Open red bin to be replaced with locked red bin in forging area
810_Occurance_After.jpeg
Outflow (Before) N/A
810_Outflow_Before.png
Outflow (After) Micro crack detection regarding training to be given to NPC final inspection inspectors. & Q -Alert to be displayed at the final Q-gate
810_Outflow_After.png
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant All similar model
 
12. Document Review
Documents PFMEA, WISOP
Specify Other Document NA
 
13. Effectiveness Of Action
Reviewed Quantity 100
Reason for submission ok