QFR No - 8000874661
Defect Details
NC No. 8000874661
NC Date 16/05/2024
NC Submission Date
Part No. F2DZ10910B
Part Name FORK BOLT Ø33 SPD
Supplier Name & Code 100002-CAST AND ALLOYS
ETL Plant 1118-ETL E-92,93 Suspension
Defect Details THREADING NOT OK-THREADE M12X16H UNDER SIZE
 
1. Problem Description
Defect Description M12 Threading under size
Detection Stage Receipt
Problem Severity Fitment
NG Quantity 115
Is Defect Repeatative? No
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID niyati@cast-alloys.com
Plant Head/CEO Email ID shiv.k@cast-alloys.com
MD Email ID dipen@cast-alloys.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
1680
0
0
0
0
1680
Check Qty
1564
0
0
0
0
1564
NG Qty
116
0
0
0
0
116
 
Scrap 116
Rework 0
Under Deviation 0
Containment Action
100 % Checked 3 Lots after Complaint
 
3. Process Flow
Process Flow Description
At Machining Stage
 
4. Process Details
Process / Operation Machining
Outsource No
Machine / Cell CNC
Machine / Cell No. CNC
5. Problem Analysis
Type Possible Cause Fact Verification Jud
ManUntrained OperatorSkilled Manpower AvailableX
ManSOP not FollowedPart Made as per SOPX
MachineInadequate Machine ParametersMachining Parameters are Verified and Found as per Control PlanX
ToolTool Wear OutTool Condition Found SatisfactoryX
ToolWrong Tool SelectionTooling Used as per Process Parameter ChecksheetX
ManIncorrect Tool OffsetingOperator Mistake in Providing Offset for ToolO
 
6. Inspection Method Analysis (Current)
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size 5 / Batch
7. Root Cause Analysis (Occurance)
Why 1 M12X1 6 H Gauge Under Size
Why 2 During Machining .
Why 3 Incorrect Tool Offset .
Why 4 Operator Error Mistake During Offset Setting .
Why 5
Root Cause (Occurance) Operator Error Mistake During Offset Setting .
 
Root Cause Analysis (Outflow)
Why 1 M12X1 6 H Gauge Under Size
Why 2 Missed at Final Inspection stage`
Why 3 Sampling Base Inspection at FI Stage
Why 4
Why 5
Root Cause (Outflow) Sampling Base Inspection at FI Stage
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
Occurance1. Retraining Provided to Machining Operator. 2. Supervisor to verify the part after providing any offset .Naitik Vachani19/05/202419/05/2024Completed
Outflow100 % Inspection Started at Machining Stage & At Final Inspection Stage Three Lots to be 100% VerifiedNitin Chaudhari19/05/202419/05/2024Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details 100% Inspection Started at Machining Stage
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size 5 / Batch
10. Evidance of Countermeasure
Occurance (Before)
Occurance (After)
Outflow (Before)
Outflow (After)
 
11. Horizontal Deployment
Horizontal Deployment Required
Applicable Machine / Model / Plant
 
12. Document Review
Documents
Specify Other Document
 
13. Effectiveness Of Action
Reviewed Quantity
Reason for submission