QFR No - 8000874661
Defect Details
NC No. | 8000874661 |
NC Date | 16/05/2024 |
NC Submission Date | |
Part No. | F2DZ10910B |
Part Name | FORK BOLT Ø33 SPD |
Supplier Name & Code | 100002-CAST AND ALLOYS |
ETL Plant | 1118-ETL E-92,93 Suspension |
Defect Details | THREADING NOT OK-THREADE M12X16H UNDER SIZE |
1. Problem Description
Defect Description | M12 Threading under size |
Detection Stage | Receipt |
Problem Severity | Fitment |
NG Quantity | 115 |
Is Defect Repeatative? | No |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | niyati@cast-alloys.com |
Plant Head/CEO Email ID | shiv.k@cast-alloys.com |
MD Email ID | dipen@cast-alloys.com |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
1680
|
0
|
0
|
0
|
0
|
1680
|
Check Qty |
1564
|
0
|
0
|
0
|
0
|
1564
|
NG Qty |
116
|
0
|
0
|
0
|
0
|
116
|
Scrap | 116 |
Rework | 0 |
Under Deviation | 0 |
Containment Action |
---|
100 % Checked 3 Lots after Complaint |
3. Process Flow
Process Flow Description |
---|
At Machining Stage |
4. Process Details
Process / Operation | Machining |
Outsource | No |
Machine / Cell | CNC |
Machine / Cell No. | CNC |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Man | Untrained Operator | Skilled Manpower Available | X |
Man | SOP not Followed | Part Made as per SOP | X |
Machine | Inadequate Machine Parameters | Machining Parameters are Verified and Found as per Control Plan | X |
Tool | Tool Wear Out | Tool Condition Found Satisfactory | X |
Tool | Wrong Tool Selection | Tooling Used as per Process Parameter Checksheet | X |
Man | Incorrect Tool Offseting | Operator Mistake in Providing Offset for Tool | O |
6. Inspection Method Analysis (Current)
Inspection Method | Gauge |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | Sampling |
Sampling | No |
Sample Size | 5 / Batch |
7. Root Cause Analysis (Occurance)
Why 1 | M12X1 6 H Gauge Under Size |
Why 2 | During Machining . |
Why 3 | Incorrect Tool Offset . |
Why 4 | Operator Error Mistake During Offset Setting . |
Why 5 | |
Root Cause (Occurance) | Operator Error Mistake During Offset Setting . |
Root Cause Analysis (Outflow)
Why 1 | M12X1 6 H Gauge Under Size |
Why 2 | Missed at Final Inspection stage` |
Why 3 | Sampling Base Inspection at FI Stage |
Why 4 | |
Why 5 | |
Root Cause (Outflow) | Sampling Base Inspection at FI Stage |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Occurance | 1. Retraining Provided to Machining Operator. 2. Supervisor to verify the part after providing any offset . | Naitik Vachani | 19/05/2024 | 19/05/2024 | Completed |
Outflow | 100 % Inspection Started at Machining Stage & At Final Inspection Stage Three Lots to be 100% Verified | Nitin Chaudhari | 19/05/2024 | 19/05/2024 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | Yes |
Change Details | 100% Inspection Started at Machining Stage |
Inspection Method | Gauge |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | Sampling |
Sampling | No |
Sample Size | 5 / Batch |
10. Evidance of Countermeasure
Occurance (Before) |
|
Occurance (After) |
|
Outflow (Before) |
|
Outflow (After) |
|
11. Horizontal Deployment
Horizontal Deployment Required | |
Applicable Machine / Model / Plant |
12. Document Review
Documents | |
Specify Other Document |
13. Effectiveness Of Action
Reviewed Quantity | |
Reason for submission |