QFR No - 8000875383
Defect Details
NC No. 8000875383
NC Date 24/05/2024
NC Submission Date
Part No. S2DC06502B
Part Name INNER DUST COVER (L=86)
Supplier Name & Code 100990-JAIRAJ ANCILLARIES PVT LTD
ETL Plant 1118-ETL E-92,93 Suspension
Defect Details EXCESS MATERIAL-MATIRAL DEFT
 
1. Problem Description
Defect Description Do Spot
Detection Stage Receipt
Problem Severity Safety
NG Quantity 1140
Is Defect Repeatative? Yes
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID planthead.aurangabad@jairajgroup.com
Plant Head/CEO Email ID vp@jairajgroup.com
MD Email ID rajiv@jairajgroup.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
2600
0
0
985
0
3585
Check Qty
2600
0
0
985
0
3585
NG Qty
1140
0
0
48
0
1188
 
Scrap 1188
Rework 0
Under Deviation 0
Containment Action
Checked 100 % parts available at ETL line & in stores on 25.5.2024. Also checked 100 % stock available at inhouse FG stores on 25.5.2024
 
3. Process Flow
Process Flow Description
Receipt of Material, Inward inspection, Storage, Material issue, Master batch mixing, Injection molding, Deflashing & Inspection, Final Inspection, Packaging & labelling, Pre dispatch Inspection, Dispatch
 
4. Process Details
Process / Operation Injection Moulding
Outsource No
Machine / Cell Injection Moulding Cell
Machine / Cell No. IMM-07
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MethodSampling inspectionVerified & found that visual defects are checked on sampling basis at FIX
ManAwareness lacking about the defectVerified that operator, In process inspectors & final inspectors lacks the awareness about the defeX
MachineInjection speed is highVerified as per C.P.& OCS found OK as per standard specificationO
MachineBarrel Temp low/HighVerified as per C.P.& OCS found OK as per standard specificationO
MachineBack pressure is lowVerified as per C.P. & OCS found OK as per standard specificationO
MethodRM preheating not doneVerified as per CP & OCS found that preheating not requiredO
MaterialRM grade not OKChecked with MTC and found OK as per specificationO
ToolAir trapped / Air vent inefficientVerified mold vent condition on punch side and found rust /dirt inside air vents are not cleanX
MachineMachine not working in OK conditionVerified and found that Machine working in OK conditionO
 
6. Inspection Method Analysis (Current)
Inspection Method Other
Other Inspection Method Visual
Check Point at Final Inspection No
Checking Freq. Sampling
Sampling No
Sample Size plan
7. Root Cause Analysis (Occurance)
Why 1 Bubbles observed on the part surface
Why 2 Air not coming out of the mold during molding process
Why 3 Air trapped inside the system during the process
Why 4 Air vents are not fully open/ cleaned
Why 5 Cleaning done during PM is not effective
Root Cause (Occurance) Air vent cleaning done during PM is not effective
 
Root Cause Analysis (Outflow)
Why 1 Bubbles observed on the part surface
Why 2 Defective part skipped from operator & inspectors
Why 3 Less awareness of operator & inspectors about the defect
Why 4 Point not added in In-process inspection check sheet, set up approval report & Inspection standard sheet
Why 5
Root Cause (Outflow) Less awareness of operator & inspectors about the defect
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceAir vent cleaning done by chemical WD-40Mr. Ganesh Mhaske30/05/2024Completed
OccuranceDuring PM of mold, air vent cleaning by chemical WD-40 is now introduced to enhance the effectiveness of cleaning ,point added in mold PM check sheetSandeep Roday30/05/2024Completed
OutflowPoint added in In-process check sheet, Set up approval report, Control Plan, PFMEASandeep Roday31/05/2024Completed
OutflowTraining provided to operator & inspectors about the defect through OPL & Inspection standard sheetSandeep Roday30/05/2024Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details 100 % Visual inspection at Final stage for bubble defect
Inspection Method Other
Other Inspection Method Visual
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
10. Evidance of Countermeasure
Occurance (Before) Air vent cleaning not by chemical in Mould PM check sheet
819_Occurance_Before.png
Occurance (After) Air vent cleaning by chemical point added in Mould PM check sheet
819_Occurance_After.png
Outflow (Before) Point of Bubble checking not addressed in Inspection standard check sheet
819_Outflow_Before.png
Outflow (After) Point of Bubble checking addressed in Inspection standard check sheet & OPL displayed
819_Outflow_After.png
 
11. Horizontal Deployment
Horizontal Deployment Required No
Applicable Machine / Model / Plant NO
 
12. Document Review
Documents ControlPlan, PMCheckSheet, PFMEA, InspCheckSheet
Specify Other Document Set up Approval Repo
 
13. Effectiveness Of Action
Reviewed Quantity 10000
Reason for submission no any concern observed after action taken.