QFR No - 8000875383
Defect Details
NC No. | 8000875383 |
NC Date | 24/05/2024 |
NC Submission Date | |
Part No. | S2DC06502B |
Part Name | INNER DUST COVER (L=86) |
Supplier Name & Code | 100990-JAIRAJ ANCILLARIES PVT LTD |
ETL Plant | 1118-ETL E-92,93 Suspension |
Defect Details | EXCESS MATERIAL-MATIRAL DEFT |
1. Problem Description
Defect Description | Do Spot |
Detection Stage | Receipt |
Problem Severity | Safety |
NG Quantity | 1140 |
Is Defect Repeatative? | Yes |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | planthead.aurangabad@jairajgroup.com |
Plant Head/CEO Email ID | vp@jairajgroup.com |
MD Email ID | rajiv@jairajgroup.com |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
2600
|
0
|
0
|
985
|
0
|
3585
|
Check Qty |
2600
|
0
|
0
|
985
|
0
|
3585
|
NG Qty |
1140
|
0
|
0
|
48
|
0
|
1188
|
Scrap | 1188 |
Rework | 0 |
Under Deviation | 0 |
Containment Action |
---|
Checked 100 % parts available at ETL line & in stores on 25.5.2024. Also checked 100 % stock available at inhouse FG stores on 25.5.2024 |
3. Process Flow
Process Flow Description |
---|
Receipt of Material, Inward inspection, Storage, Material issue, Master batch mixing, Injection molding, Deflashing & Inspection, Final Inspection, Packaging & labelling, Pre dispatch Inspection, Dispatch |
4. Process Details
Process / Operation | Injection Moulding |
Outsource | No |
Machine / Cell | Injection Moulding Cell |
Machine / Cell No. | IMM-07 |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Method | Sampling inspection | Verified & found that visual defects are checked on sampling basis at FI | X |
Man | Awareness lacking about the defect | Verified that operator, In process inspectors & final inspectors lacks the awareness about the defe | X |
Machine | Injection speed is high | Verified as per C.P.& OCS found OK as per standard specification | O |
Machine | Barrel Temp low/High | Verified as per C.P.& OCS found OK as per standard specification | O |
Machine | Back pressure is low | Verified as per C.P. & OCS found OK as per standard specification | O |
Method | RM preheating not done | Verified as per CP & OCS found that preheating not required | O |
Material | RM grade not OK | Checked with MTC and found OK as per specification | O |
Tool | Air trapped / Air vent inefficient | Verified mold vent condition on punch side and found rust /dirt inside air vents are not clean | X |
Machine | Machine not working in OK condition | Verified and found that Machine working in OK condition | O |
6. Inspection Method Analysis (Current)
Inspection Method | Other |
Other Inspection Method | Visual |
Check Point at Final Inspection | No |
Checking Freq. | Sampling |
Sampling | No |
Sample Size | plan |
7. Root Cause Analysis (Occurance)
Why 1 | Bubbles observed on the part surface |
Why 2 | Air not coming out of the mold during molding process |
Why 3 | Air trapped inside the system during the process |
Why 4 | Air vents are not fully open/ cleaned |
Why 5 | Cleaning done during PM is not effective |
Root Cause (Occurance) | Air vent cleaning done during PM is not effective |
Root Cause Analysis (Outflow)
Why 1 | Bubbles observed on the part surface |
Why 2 | Defective part skipped from operator & inspectors |
Why 3 | Less awareness of operator & inspectors about the defect |
Why 4 | Point not added in In-process inspection check sheet, set up approval report & Inspection standard sheet |
Why 5 | |
Root Cause (Outflow) | Less awareness of operator & inspectors about the defect |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Occurance | Air vent cleaning done by chemical WD-40 | Mr. Ganesh Mhaske | 30/05/2024 | Completed | |
Occurance | During PM of mold, air vent cleaning by chemical WD-40 is now introduced to enhance the effectiveness of cleaning ,point added in mold PM check sheet | Sandeep Roday | 30/05/2024 | Completed | |
Outflow | Point added in In-process check sheet, Set up approval report, Control Plan, PFMEA | Sandeep Roday | 31/05/2024 | Completed | |
Outflow | Training provided to operator & inspectors about the defect through OPL & Inspection standard sheet | Sandeep Roday | 30/05/2024 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | Yes |
Change Details | 100 % Visual inspection at Final stage for bubble defect |
Inspection Method | Other |
Other Inspection Method | Visual |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100% |
10. Evidance of Countermeasure
Occurance (Before) |
Air vent cleaning not by chemical in Mould PM check sheet 819_Occurance_Before.png |
Occurance (After) |
Air vent cleaning by chemical point added in Mould PM check sheet 819_Occurance_After.png |
Outflow (Before) |
Point of Bubble checking not addressed in Inspection standard check sheet 819_Outflow_Before.png |
Outflow (After) |
Point of Bubble checking addressed in Inspection standard check sheet & OPL displayed 819_Outflow_After.png |
11. Horizontal Deployment
Horizontal Deployment Required | No |
Applicable Machine / Model / Plant | NO |
12. Document Review
Documents | ControlPlan, PMCheckSheet, PFMEA, InspCheckSheet |
Specify Other Document | Set up Approval Repo |
13. Effectiveness Of Action
Reviewed Quantity | 10000 |
Reason for submission | no any concern observed after action taken. |