QFR No - 8000876571
Defect Details
NC No. 8000876571
NC Date 30/05/2024
NC Submission Date
Part No. 165FG01101
Part Name GEAR PRIMARY ASSLY 3W-4S 200 cc LPG
Supplier Name & Code 100237-SANJEEV AUTO PARTS MRFS PVT LT
ETL Plant 1132-ETL K-226/1 TRANSMISSION
Defect Details MIX UP OTHER MODEL-WRONG HOBBING ISSUE (77TEETH)
 
1. Problem Description
Defect Description Wrong teeth Hobbing done (77 teeth Hobbing done instead of 74 Nos)
Detection Stage Inprocess
Problem Severity Fitment
NG Quantity 1
Is Defect Repeatative? Yes
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID vpwankhade@sanjeevgroup.com
Plant Head/CEO Email ID rmtiwari@sanjeevgroup.com
MD Email ID maithilee@sanjeevgroup.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
200
0
0
210
240
650
Check Qty
200
0
0
210
240
650
NG Qty
0
0
0
0
0
0
 
Scrap 0
Rework 0
Under Deviation 0
Containment Action
100% material checked at WIP &Final inspection confirmation with tick mark identification to ensure defect free parts.
 
3. Process Flow
Process Flow Description
Raw Material Inward Bar Cutting Billet Heating Hot Forging Normalizing Shotblasting Coining Preturning Peircing-1 Peircing-2 Shaving-1 Shaving-2 Milling-1 Milling-2 Finish turning 1st setup Finish turning 2nd setup Finish turning 3rd setup Deburring Final Inspection CNC Blank Inward Inspection CNC Blank Traciability Marking Hobbing Teeth Chamfering Gear Shaving Heat tratment Shotblasting ID Turning Bush Pressing Bush Turning Washing Final inspection
 
4. Process Details
Process / Operation Hobbing
Outsource No
Machine / Cell GPH Cell
Machine / Cell No. Glesson -1
5. Problem Analysis
Type Possible Cause Fact Verification Jud
Manmaterial mixup with GPH single groove in GPH double grooveDuring hobbing part loading visaul inspection to be done.O
 
6. Inspection Method Analysis (Current)
Inspection Method Other
Other Inspection Method Visual
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
7. Root Cause Analysis (Occurance)
Why 1 MIX UP OTHER MODEL-WRONG HOBBING ISSUE (77 TEETH)
Why 2 WRONG CNC BLANKLOADED FOR HOBBING
Why 3 VERIFICATION OF BLANK NOT DONE BEFORE LOADING FOR HOBBING
Why 4 VERIFICATION (INPECTION) SKIPPED
Why 5 NA
Root Cause (Occurance) VERIFICATION (INPECTION) SKIPPED
 
Root Cause Analysis (Outflow)
Why 1 MIX UP OTHER MODEL-WRONG HOBBING ISSUE (77 TEETH)
Why 2 Not arrested during DFCE inspection
Why 3 Dail pressure scale value inspection skipped during DFCE Inspection.
Why 4 NA
Why 5 NA
Root Cause (Outflow) Dail pressure scale value inspection skipped during DFCE Inspection.
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceOPL DISPLAYED AT HOBBINGVGW04/06/202404/06/2024Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details Visual Inspection
Inspection Method Other
Other Inspection Method Visual Inspection
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
10. Evidance of Countermeasure
Occurance (Before) Wrong part loaded during hobbing verification skipped
831_Occurance_Before.pdf
Occurance (After) Q-Alert dispayed at hobbing sytage for identification of CNC parts.
831_Occurance_After.pdf
Outflow (Before) Dial pressure scale value inspection skipped durong inspection
831_Outflow_Before.pdf
Outflow (After) Q-Alert dispayed at Final inspection stage for inspection of dial pressure scale value
831_Outflow_After.pdf
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant ALL GPH Family
 
12. Document Review
Documents
Specify Other Document Q-Alert Dispalyed
 
13. Effectiveness Of Action
Reviewed Quantity 2000
Reason for submission Repeated Quality issue -POKA YOKE required in Machine (Possibility of customer Complaint) Also outflow action missing