QFR No - 8000876969
Defect Details
NC No. | 8000876969 |
NC Date | 05/06/2024 |
NC Submission Date | |
Part No. | F2FA11933B |
Part Name | FORK PIPE MACHINED - J1D |
Supplier Name & Code | 101030-TUBE INVESTMENTS OF INDIA LTD |
ETL Plant | 1117-ETL K-228/9 Suspension |
Defect Details | NOT AS PER SPECIFICATION-SHORT LENGTH |
1. Problem Description
Defect Description | SHORT LENGTH |
Detection Stage | Receipt |
Problem Severity | Fitment |
NG Quantity | 7 |
Is Defect Repeatative? | Yes |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | AmitVD@tii.murugappa.com |
Plant Head/CEO Email ID | guptaajay@tii.murugappa.com |
MD Email ID | mukeshahuja@tii.murugappa.com |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
500
|
0
|
0
|
1000
|
0
|
1500
|
Check Qty |
500
|
0
|
0
|
1000
|
0
|
1500
|
NG Qty |
7
|
0
|
0
|
4
|
0
|
11
|
Scrap | 11 |
Rework | 0 |
Under Deviation | 0 |
Containment Action |
---|
All Stock available at ETL end & Inhouse checked for the Threading Parameter |
3. Process Flow
Process Flow Description |
---|
Raw Material Inspection- Machining (Cualking & Threading)-Drilling-Oiling-Final Inspection-Dispatch |
4. Process Details
Process / Operation | Machining |
Outsource | No |
Machine / Cell | CNC Machine Cell |
Machine / Cell No. | M/c No. 22 |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|
6. Inspection Method Analysis (Current)
Inspection Method | Gauge |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | Sampling |
Sampling | No |
Sample Size | 20 nos |
7. Root Cause Analysis (Occurance)
Why 1 | Total Length Observed Undersize |
Why 2 | Tube end face not resting properly on Stopper Surface |
Why 3 | The uneven resting surface of the stopper |
Why 4 | During Mass production resting surface of the stopper wears out |
Why 5 | The current Stopper, material used was MS & Not enough which caused the stopper wear out |
Root Cause (Occurance) | The current Stopper, material used was MS & Not enough which caused the stopper wear out |
Root Cause Analysis (Outflow)
Why 1 | Not Detected during the Final Inspection & PDIR |
Why 2 | Inspection on the Sampling Basis |
Why 3 | No Length Inspection gauge is available for the 100 % Inspection |
Why 4 | |
Why 5 | |
Root Cause (Outflow) | No Length Inspection gauge is available for the 100 % Inspection |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Outflow | add new height checking gauge | dethe s s | 15/06/2024 | 08/06/2024 | Completed |
Occurance | Monitoring Started for the Stopper condition Verification during the JH Maintenance which not in practice Erlier | Mr. Dethe SS | 14/06/2024 | 08/06/2024 | Completed |
Occurance | The Carbide material was used for the new stopper & made Properly hard (50 to 65 HB ) & to prevent loose burr from sticking to the stopper, Also Provision was made for the coolant to come out from the stopper. | Mr. Rathod KS | 03/07/2024 | 03/07/2024 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | Yes |
Change Details | Length Inspection Gauge Added for the 100 % Inspection |
Inspection Method | Gauge |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100 % |
10. Evidance of Countermeasure
Occurance (Before) |
The current Stopper, material used was MS & Not enough which caused the stopper to wear out 836_Occurance_Before.pdf |
Occurance (After) |
The Carbide material was used for the new stopper & made Properly hard (50 to 65 HB ) & to prevent loose burr from sticking to the stopper, Also Provision was made for the coolant to come out from the stopper. 836_Occurance_After.pdf |
Outflow (Before) |
Before: No 100 % Inspection on Length Gauge 836_Outflow_Before.pdf |
Outflow (After) |
After: 100 % Inspection Started by Using Length Inspection Gauge 836_Outflow_After.pdf |
11. Horizontal Deployment
Horizontal Deployment Required | Yes |
Applicable Machine / Model / Plant | All Model |
12. Document Review
Documents | WISOP, JHCheckSheet |
Specify Other Document | WI |
13. Effectiveness Of Action
Reviewed Quantity | 150 |
Reason for submission | 1. How much stopper life earlier & now 2. WI for what purpose revised (WI not attached) |