QFR No - 8000877797
Defect Details
NC No. | 8000877797 |
NC Date | 11/06/2024 |
NC Submission Date | |
Part No. | F2LG05402B |
Part Name | SEAT PIPE - J1A & J1D |
Supplier Name & Code | 100539-N P ENTERPRISES |
ETL Plant | 1117-ETL K-228/9 Suspension |
Defect Details | NOT AS PER SPECIFICATION-ID STEP |
1. Problem Description
Defect Description | ID STEP |
Detection Stage | Inprocess |
Problem Severity | Fitment |
NG Quantity | 3 |
Is Defect Repeatative? | Yes |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | quality@npcindustries.in |
Plant Head/CEO Email ID | anand@npcindustries.in |
MD Email ID | ajay@npcindustries.in |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
2080
|
46000
|
0
|
0
|
0
|
48080
|
Check Qty |
2080
|
46000
|
0
|
0
|
0
|
48080
|
NG Qty |
3
|
23
|
0
|
0
|
0
|
26
|
Scrap | 26 |
Rework | 0 |
Under Deviation | 0 |
Containment Action |
---|
Segregate all material at both end |
3. Process Flow
Process Flow Description |
---|
Process Flow Description 1.0 Raw Material 2.0 Cutting 3.0 Drawing 4.0 Head Formation 5.0 Rough Grinding 6.0 Punching 7.0 CNC Head Turning 8.0 CNC Boring & Facing 9.0 Tapping 10.0 Chamfering 11.0 ID Deburring 12.0 Finish Grinding 13.0 Final Inspection 14.0 Cleaning 15.0 Oiling 16.0 Packing &Dispatch. |
4. Process Details
Process / Operation | Forging |
Outsource | No |
Machine / Cell | Header |
Machine / Cell No. | MDM-8 |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Man | Operator negligence | Operator found to be non negligent | O |
Machine | Non detection of material unclear in ID at final Inspection | Material unclear in ID could not be detected at final inspection | X |
Tool | Damage of Pin at Forging | Pin was found to be damaged which lead to accumulation of material in ID | X |
Machine | Variation in Forging machine | No variation in Forging machine found | O |
Material | Material composition not OK | Material composition found to be OK | O |
6. Inspection Method Analysis (Current)
Inspection Method | Other |
Other Inspection Method | Visual |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100% |
7. Root Cause Analysis (Occurance)
Why 1 | Step in ID |
Why 2 | accumulation of material in ID |
Why 3 | Forging Pin got damaged |
Why 4 | Miss alignment of PC clamping finger on the forging machine. |
Why 5 | The spring`s clamping finger was loose. |
Root Cause (Occurance) | The spring`s clamping finger was loose. |
Root Cause Analysis (Outflow)
Why 1 | Step in ID |
Why 2 | Could not be detected at final inspection |
Why 3 | ID step checkpoint not available at final inspection |
Why 4 | |
Why 5 | |
Root Cause (Outflow) | ID step checkpoint not available at final inspection |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Outflow | Sampling Inspection to started with the plug gauge at the final inspection. | Mr. Ankush | 15/06/2024 | 12/06/2024 | Completed |
Occurance | clamping finger Inspection checkpoint to be added in Daily machine checksheet. | Mr. Princ | 15/06/2024 | 14/06/2024 | Completed |
Occurance | Quality Alert to be displayed in Forging Shop | Mr. Prince | 12/06/2024 | 11/06/2024 | Completed |
Outflow | Quality Alert to be displayed at Final Inspection. | Mr. Princ | 12/06/2024 | 11/06/2024 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | Yes |
Change Details | The part should be inspected using a plug gauge and undergo 100% visual inspection. |
Inspection Method | Gauge |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | Sampling |
Sampling | No |
Sample Size | As per std |
10. Evidance of Countermeasure
Occurance (Before) |
clamping finger Inspection was not done at daily basis. 841_Occurance_Before.jpg |
Occurance (After) |
clamping finger Inspection checkpoint to be added in Daily machine check sheet. 841_Occurance_After.jpg |
Outflow (Before) |
Only Visual Inspection but Step id checkpoint not available. 841_Outflow_Before.png |
Outflow (After) |
Sampling Inspection to started with the plug gauge at the final inspection. 841_Outflow_After.jpg |
11. Horizontal Deployment
Horizontal Deployment Required | Yes |
Applicable Machine / Model / Plant | Header |
12. Document Review
Documents | ControlPlan, PFMEA, JHCheckSheet, InspCheckSheet |
Specify Other Document | NO |
13. Effectiveness Of Action
Reviewed Quantity | 100 |
Reason for submission | ok |