QFR No - 8000877797
Defect Details
NC No. 8000877797
NC Date 11/06/2024
NC Submission Date
Part No. F2LG05402B
Part Name SEAT PIPE - J1A & J1D
Supplier Name & Code 100539-N P ENTERPRISES
ETL Plant 1117-ETL K-228/9 Suspension
Defect Details NOT AS PER SPECIFICATION-ID STEP
 
1. Problem Description
Defect Description ID STEP
Detection Stage Inprocess
Problem Severity Fitment
NG Quantity 3
Is Defect Repeatative? Yes
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID quality@npcindustries.in
Plant Head/CEO Email ID anand@npcindustries.in
MD Email ID ajay@npcindustries.in
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
2080
46000
0
0
0
48080
Check Qty
2080
46000
0
0
0
48080
NG Qty
3
23
0
0
0
26
 
Scrap 26
Rework 0
Under Deviation 0
Containment Action
Segregate all material at both end
 
3. Process Flow
Process Flow Description
Process Flow Description 1.0 Raw Material 2.0 Cutting 3.0 Drawing 4.0 Head Formation 5.0 Rough Grinding 6.0 Punching 7.0 CNC Head Turning 8.0 CNC Boring & Facing 9.0 Tapping 10.0 Chamfering 11.0 ID Deburring 12.0 Finish Grinding 13.0 Final Inspection 14.0 Cleaning 15.0 Oiling 16.0 Packing &Dispatch.
 
4. Process Details
Process / Operation Forging
Outsource No
Machine / Cell Header
Machine / Cell No. MDM-8
5. Problem Analysis
Type Possible Cause Fact Verification Jud
ManOperator negligenceOperator found to be non negligentO
MachineNon detection of material unclear in ID at final InspectionMaterial unclear in ID could not be detected at final inspectionX
ToolDamage of Pin at ForgingPin was found to be damaged which lead to accumulation of material in IDX
MachineVariation in Forging machineNo variation in Forging machine foundO
MaterialMaterial composition not OKMaterial composition found to be OKO
 
6. Inspection Method Analysis (Current)
Inspection Method Other
Other Inspection Method Visual
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
7. Root Cause Analysis (Occurance)
Why 1 Step in ID
Why 2 accumulation of material in ID
Why 3 Forging Pin got damaged
Why 4 Miss alignment of PC clamping finger on the forging machine.
Why 5 The spring`s clamping finger was loose.
Root Cause (Occurance) The spring`s clamping finger was loose.
 
Root Cause Analysis (Outflow)
Why 1 Step in ID
Why 2 Could not be detected at final inspection
Why 3 ID step checkpoint not available at final inspection
Why 4
Why 5
Root Cause (Outflow) ID step checkpoint not available at final inspection
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OutflowSampling Inspection to started with the plug gauge at the final inspection.Mr. Ankush15/06/202412/06/2024Completed
Occuranceclamping finger Inspection checkpoint to be added in Daily machine checksheet.Mr. Princ15/06/202414/06/2024Completed
OccuranceQuality Alert to be displayed in Forging ShopMr. Prince12/06/202411/06/2024Completed
OutflowQuality Alert to be displayed at Final Inspection.Mr. Princ12/06/202411/06/2024Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details The part should be inspected using a plug gauge and undergo 100% visual inspection.
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size As per std
10. Evidance of Countermeasure
Occurance (Before) clamping finger Inspection was not done at daily basis.
841_Occurance_Before.jpg
Occurance (After) clamping finger Inspection checkpoint to be added in Daily machine check sheet.
841_Occurance_After.jpg
Outflow (Before) Only Visual Inspection but Step id checkpoint not available.
841_Outflow_Before.png
Outflow (After) Sampling Inspection to started with the plug gauge at the final inspection.
841_Outflow_After.jpg
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant Header
 
12. Document Review
Documents ControlPlan, PFMEA, JHCheckSheet, InspCheckSheet
Specify Other Document NO
 
13. Effectiveness Of Action
Reviewed Quantity 100
Reason for submission ok