QFR No - 8000877824
Defect Details
NC No. | 8000877824 |
NC Date | 11/06/2024 |
NC Submission Date | |
Part No. | F2LG07702B |
Part Name | SEAT PIPE - J1C2 FF |
Supplier Name & Code | 100539-N P ENTERPRISES |
ETL Plant | 1117-ETL K-228/9 Suspension |
Defect Details | NOT AS PER SPECIFICATION-GROOVE DIA. OVERSIZE |
1. Problem Description
Defect Description | GROOVE DIA. OVERSIZE |
Detection Stage | Inprocess |
Problem Severity | Fitment |
NG Quantity | 13 |
Is Defect Repeatative? | Yes |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | quality@npcindustries.in |
Plant Head/CEO Email ID | anand@npcindustries.in |
MD Email ID | ajay@npcindustries.in |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
960
|
14000
|
0
|
0
|
0
|
14960
|
Check Qty |
960
|
14000
|
0
|
0
|
0
|
14960
|
NG Qty |
13
|
0
|
0
|
0
|
0
|
13
|
Scrap | 0 |
Rework | 13 |
Under Deviation | 0 |
Containment Action |
---|
segregate all material at both end |
3. Process Flow
Process Flow Description |
---|
Process Flow Description 1.0 Raw Material 2.0 Cutting 3.0 Drawing 4.0 Head Formation 5.0 Rough Grinding 6.0 Punching 7.0 CNC Head Turning 8.0 CNC Boring & Facing 9.0 Tapping 10.0 Chamfering 11.0 ID Deburring 12.0 Finish Grinding 13.0 Final Inspection 14.0 Cleaning 15.0 Oiling 16.0 Packing &Dispatch. |
4. Process Details
Process / Operation | CNC Head Turning |
Outsource | No |
Machine / Cell | CNC |
Machine / Cell No. | BC-CNC-21 |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Man | Operator unaware | Operator found to be aware about the process | O |
Man | Negligence of quality inspector at in process | Quality inspector found to be non negligent . | O |
Tool | Damage of Grooving Insert | It was verified and observed that Grooving Insert got damaged which resulted in width becoming under | X |
Tool | Forging dia over | Forging dia observed to be correct. No linkage with defect observed | O |
Machine | Wrong program selection | It was verified that correct program was selected for machining. | O |
Method | NG part skipped at Final inspection | It was verified and observed that parts skipped during sampling at final inspection | X |
Method | Improper clamping of insert | It was observed that clamping of insert is proper | O |
6. Inspection Method Analysis (Current)
Inspection Method | Other |
Other Inspection Method | Visual |
Check Point at Final Inspection | Yes |
Checking Freq. | Sampling |
Sampling | No |
Sample Size | as per std |
7. Root Cause Analysis (Occurance)
Why 1 | Groove width undersize |
Why 2 | Step observed |
Why 3 | Grooving Insert got damaged |
Why 4 | Part could not be clamped properly |
Why 5 | Rough Grinding dia down due to Rough Grinding Setting parts mixed |
Root Cause (Occurance) | Rough Grinding dia down due to Rough Grinding Setting parts mixed |
Root Cause Analysis (Outflow)
Why 1 | Groove width undersize |
Why 2 | Could not be detected at Final Inspection |
Why 3 | Skipped in Sampling inspection |
Why 4 | |
Why 5 | |
Root Cause (Outflow) | Skipped in Sampling inspection |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Occurance | Quality alert to be displayed at CNC station | Mr. Princ | 12/06/2024 | 11/06/2024 | Completed |
Outflow | Quality alert to be displayed at final inspection station | Mr. Princ | 12/06/2024 | 11/06/2024 | Completed |
Outflow | Min level 3 operator will be allowed to operate CNC Head Turning Machine | Mr. Harwinder | 14/06/2024 | 13/06/2024 | Completed |
Outflow | 100% inspection with Slip Gauge to be done before dispatch | Mr. Ankush | 13/06/2024 | 12/06/2024 | Completed |
Occurance | Rough Grinding setting parts to be quarantined in Lock & Key Bin by Quality Inspector himself | Mr. Ankush | 13/06/2024 | 12/06/2024 | Completed |
Outflow | Training to be provided to all CNC operators for abnormal sound and checking insert manually | Mr. Harwinder | 14/06/2024 | 13/06/2024 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | Yes |
Change Details | 100% inspection with Slip Gauge to be done before dispatch |
Inspection Method | Gauge |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100% |
10. Evidance of Countermeasure
Occurance (Before) |
Open redbin used for rejection pcs at rough grinder 845_Occurance_Before.jpeg |
Occurance (After) |
Locked Redbin implemented at rough grinder 845_Occurance_After.jpeg |
Outflow (Before) |
use sampling method for inspection at final Q gate 845_Outflow_Before.png |
Outflow (After) |
100 % inspection to be started with slip gauge and Q alert to be displayed at final Q gate. 845_Outflow_After.jpg |
11. Horizontal Deployment
Horizontal Deployment Required | No |
Applicable Machine / Model / Plant | Similar model |
12. Document Review
Documents | ControlPlan, PFMEA, InspCheckSheet |
Specify Other Document | No |
13. Effectiveness Of Action
Reviewed Quantity | 100 |
Reason for submission | OK |