QFR No - 8000877824
Defect Details
NC No. 8000877824
NC Date 11/06/2024
NC Submission Date
Part No. F2LG07702B
Part Name SEAT PIPE - J1C2 FF
Supplier Name & Code 100539-N P ENTERPRISES
ETL Plant 1117-ETL K-228/9 Suspension
Defect Details NOT AS PER SPECIFICATION-GROOVE DIA. OVERSIZE
 
1. Problem Description
Defect Description GROOVE DIA. OVERSIZE
Detection Stage Inprocess
Problem Severity Fitment
NG Quantity 13
Is Defect Repeatative? Yes
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID quality@npcindustries.in
Plant Head/CEO Email ID anand@npcindustries.in
MD Email ID ajay@npcindustries.in
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
960
14000
0
0
0
14960
Check Qty
960
14000
0
0
0
14960
NG Qty
13
0
0
0
0
13
 
Scrap 0
Rework 13
Under Deviation 0
Containment Action
segregate all material at both end
 
3. Process Flow
Process Flow Description
Process Flow Description 1.0 Raw Material 2.0 Cutting 3.0 Drawing 4.0 Head Formation 5.0 Rough Grinding 6.0 Punching 7.0 CNC Head Turning 8.0 CNC Boring & Facing 9.0 Tapping 10.0 Chamfering 11.0 ID Deburring 12.0 Finish Grinding 13.0 Final Inspection 14.0 Cleaning 15.0 Oiling 16.0 Packing &Dispatch.
 
4. Process Details
Process / Operation CNC Head Turning
Outsource No
Machine / Cell CNC
Machine / Cell No. BC-CNC-21
5. Problem Analysis
Type Possible Cause Fact Verification Jud
ManOperator unawareOperator found to be aware about the processO
ManNegligence of quality inspector at in processQuality inspector found to be non negligent .O
ToolDamage of Grooving InsertIt was verified and observed that Grooving Insert got damaged which resulted in width becoming underX
ToolForging dia overForging dia observed to be correct. No linkage with defect observedO
MachineWrong program selectionIt was verified that correct program was selected for machining.O
MethodNG part skipped at Final inspectionIt was verified and observed that parts skipped during sampling at final inspectionX
MethodImproper clamping of insertIt was observed that clamping of insert is properO
 
6. Inspection Method Analysis (Current)
Inspection Method Other
Other Inspection Method Visual
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size as per std
7. Root Cause Analysis (Occurance)
Why 1 Groove width undersize
Why 2 Step observed
Why 3 Grooving Insert got damaged
Why 4 Part could not be clamped properly
Why 5 Rough Grinding dia down  due to Rough Grinding Setting parts mixed
Root Cause (Occurance) Rough Grinding dia down  due to Rough Grinding Setting parts mixed
 
Root Cause Analysis (Outflow)
Why 1 Groove width undersize
Why 2 Could not be detected at Final Inspection
Why 3 Skipped in Sampling inspection
Why 4
Why 5
Root Cause (Outflow) Skipped in Sampling inspection
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceQuality alert to be displayed at CNC stationMr. Princ12/06/202411/06/2024Completed
OutflowQuality alert to be displayed at final inspection stationMr. Princ12/06/202411/06/2024Completed
OutflowMin level 3 operator will be allowed to operate CNC Head Turning MachineMr. Harwinder14/06/202413/06/2024Completed
Outflow100% inspection with Slip Gauge to be done before dispatchMr. Ankush13/06/202412/06/2024Completed
OccuranceRough Grinding setting parts to be quarantined in Lock & Key Bin by Quality Inspector himselfMr. Ankush13/06/202412/06/2024Completed
OutflowTraining to be provided to all CNC operators for abnormal sound and checking insert manuallyMr. Harwinder14/06/202413/06/2024Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details 100% inspection with Slip Gauge to be done before dispatch
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
10. Evidance of Countermeasure
Occurance (Before) Open redbin used for rejection pcs at rough grinder
845_Occurance_Before.jpeg
Occurance (After) Locked Redbin implemented at rough grinder
845_Occurance_After.jpeg
Outflow (Before) use sampling method for inspection at final Q gate
845_Outflow_Before.png
Outflow (After) 100 % inspection to be started with slip gauge and Q alert to be displayed at final Q gate.
845_Outflow_After.jpg
 
11. Horizontal Deployment
Horizontal Deployment Required No
Applicable Machine / Model / Plant Similar model
 
12. Document Review
Documents ControlPlan, PFMEA, InspCheckSheet
Specify Other Document No
 
13. Effectiveness Of Action
Reviewed Quantity 100
Reason for submission OK