QFR No - 8000877853
Defect Details
NC No. 8000877853
NC Date 11/06/2024
NC Submission Date
Part No. F2BZ05712B
Part Name CAP OIL LOCK - J1D FF (10mm taper)
Supplier Name & Code 101255-MAHAVIR INDUSTRIES
ETL Plant 1117-ETL K-228/9 Suspension
Defect Details NOT AS PER SPECIFICATION-ID OPERATION MISSING
 
1. Problem Description
Defect Description ID OPERATION MISSING
Detection Stage Inprocess
Problem Severity Fitment
NG Quantity 2
Is Defect Repeatative? No
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID quality@mahavirind.co.in
Plant Head/CEO Email ID planthead@mahavirind.co.in
MD Email ID
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
680
0
0
1280
0
1960
Check Qty
680
0
0
1280
0
1960
NG Qty
2
0
0
0
0
2
 
Scrap 2
Rework 0
Under Deviation 0
Containment Action
All Suspected Material Segregation at Customer End
 
3. Process Flow
Process Flow Description
R/M Inward- Store- Parting And Pilot drill - Bottom side chamfer-CNC Turning and ID Boring - OD Grinding - Plating - Final Inspection - Dispatch.
 
4. Process Details
Process / Operation Parting and Pilot Drill on Traub machine.
Outsource Yes
Machine / Cell Traub machine-A-25
Machine / Cell No. Traub section.
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MaterialHard MaterialCorrect Grade Material use hardness okO
ManUnskiilled Man powerSkilled operator On CNC machineO
MethodInput Material & Output Material Handling Method WrongInput and ok out put material kept On A table And Taper Ring Gauge Not available on CNC Machine .X
ToolWrong Tool use For Pilot DrillCorrect Required Tool On CNC MachineO
MachineCNC Machine Condition Not OKAs PM plan Check sheet Condition found ok .O
 
6. Inspection Method Analysis (Current)
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size 20nos
7. Root Cause Analysis (Occurance)
Why 1 NOT AS PER SPECIFICATION-ID OPERATION MISSING
Why 2 Defected Part By Mistake Mix By CNC operator
Why 3 Input material and out material Kept in one Location on CNC Machine.
Why 4
Why 5
Root Cause (Occurance) Input material and out material Kept one location on CNC Machine.
 
Root Cause Analysis (Outflow)
Why 1 NOT AS PER SPECIFICATION-ID OPERATION MISSING
Why 2 Taper Ring Gauge Not Available for 100% Taper Parameter Inspection on CNC Machine .
Why 3
Why 4
Why 5
Root Cause (Outflow) Taper Ring Gauge Not Available for 100% Taper Parameter Inspection on CNC Machine .
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceInput Material and Output material separate location Two Table Arrangement on CNC Machine .Production Head13/06/202414/06/2024Completed
OccuranceTaper Ring Gauge Provide on CNC Machine For 100% Inspection.Quality Head25/06/202425/06/2024Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details 100% Taper & ID Inspection.
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
10. Evidance of Countermeasure
Occurance (Before) Input material and out material Kept on one Table on CNC Machine.
853_Occurance_Before.jpg
Occurance (After) Now Input Material and Output material separate -separate location Two Table Arrangement on CNC Machine .
853_Occurance_After.jpg
Outflow (Before) Taper Ring Gauge Not Available for 100% Taper Parameter Inspection on CNC Machine .
853_Outflow_Before.jpg
Outflow (After) Taper Ring Gauge Provide on CNC Machine For 100% Inspection.
853_Outflow_After.jpg
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant All Cap Oil Lock
 
12. Document Review
Documents ControlPlan, PFMEA, WISOP
Specify Other Document no
 
13. Effectiveness Of Action
Reviewed Quantity 50
Reason for submission OK