QFR No - 8000878523
Defect Details
NC No. 8000878523
NC Date 15/06/2024
NC Submission Date
Part No. 550BZ01402
Part Name CAP OIL LOCK - DF01
Supplier Name & Code 101255-MAHAVIR INDUSTRIES
ETL Plant 1146-ETL Suspension Narasapura
Defect Details RUSTY-
 
1. Problem Description
Defect Description CAP OIL LOCK RUST ISSUE
Detection Stage Inprocess
Problem Severity Aesthetic
NG Quantity 616
Is Defect Repeatative? Yes
Defect Sketch / Photo bhpnhqxb2aqiqeo31315nure.gif
Supplier Communication Details
Quality Head Email ID quality@mahavirind.co.in
Plant Head/CEO Email ID production@mahavirind.co.in
MD Email ID
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
6000
0
0
0
12000
18000
Check Qty
6000
0
0
0
12000
18000
NG Qty
616
0
0
0
0
616
 
Scrap 0
Rework 616
Under Deviation 0
Containment Action
All Material Check at the Customer End and Warehouse End
 
3. Process Flow
Process Flow Description
RM inward - store - Parting Piot Drill on Traub Machine - Bottom Side Chamfer -Semi finish Inward - CNC ( Counter ID Machining ) - OD Grinding - Plating - Final Inspection - Packing - Dispatch
 
4. Process Details
Process / Operation Warehouse Loading - Unloading Handling Problem
Outsource Yes
Machine / Cell Narsapura Warehouse
Machine / Cell No. Narsapura Warehouse
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MethodFinish material Not Proper PackingYes , at Transport and Godown material not proper handlingX
 
6. Inspection Method Analysis (Current)
Inspection Method Other
Other Inspection Method Visual
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
7. Root Cause Analysis (Occurance)
Why 1 Rusty
Why 2 Finish Good Material Wet at warehouse
Why 3 Finish Good Lying On Shop floor
Why 4 Packing Bag Torn of finish good
Why 5 Finish Material Improper Material Handling
Root Cause (Occurance) Packing Bag Torn of finish good Material During Store Area as it is material collect by godown man and Dispatch.
 
Root Cause Analysis (Outflow)
Why 1 Rusty
Why 2 Finish Good Material More No. of days lying at transport Godown
Why 3 Inform To godown person
Why 4
Why 5
Root Cause (Outflow) Finish Good Material More No. of days lying at transport Godown
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
Occurance1)Improper Material Handling .2)Finish Good Material More No. of days lying at transport GodownMahavir QA25/06/202426/06/2024Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details 1)Packing as per Customer Standards. 2) HDPE white, Heavy thickness and clean Gunny bags use for outer coating packing.
Inspection Method Other
Other Inspection Method Packing Visual Obs
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
10. Evidance of Countermeasure
Occurance (Before) Finish Good Packing Bag Torn at warehouse during Material Handling .2)Low Thickness Poly Bag
873_Occurance_Before.gif
Occurance (After) 1)Inner poly bag thickness increases up to 100mic gauge Instead of 75Microm for Tearing problems avoid Suitable to Material Handling. 2)HDPE white , Heavy thickness and clean Gunny bags use for outer coating packing.
873_Occurance_After.jpg
Outflow (Before) Finish Good Material More No. of days lying at transport godown
873_Outflow_Before.xlsx
Outflow (After) As per the attached packing standard 443_Outflow_After.xlsx
873_Outflow_After.xlsx
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant All Cap Oil Lock Models
 
12. Document Review
Documents ControlPlan, PFMEA, PackingStd
Specify Other Document no
 
13. Effectiveness Of Action
Reviewed Quantity 15000
Reason for submission reviewed 2 lots found ok