QFR No - 8000879488
Defect Details
NC No. 8000879488
NC Date 22/06/2024
NC Submission Date
Part No. F1LG00902B
Part Name SEAT PIPE -K86A
Supplier Name & Code 100538-NARINDER PARKASH AND CO
ETL Plant 1146-ETL Suspension Narasapura
Defect Details HOLE BLOCK-TENSION HOLE BLOCK
 
1. Problem Description
Defect Description K86 seat pipe tension hole block issue
Detection Stage Inprocess
Problem Severity Function
NG Quantity 3
Is Defect Repeatative? Yes
Defect Sketch / Photo i2z4kjrrzalkbmbwopa4sgmv.gif
Supplier Communication Details
Quality Head Email ID quality@npcindustries.in
Plant Head/CEO Email ID anand@npcindustries.in
MD Email ID ajay@npcindustries.in
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
9000
15600
0
1500
2500
28600
Check Qty
9000
15600
0
0
0
24600
NG Qty
25
36
0
0
0
61
 
Scrap 0
Rework 61
Under Deviation 0
Containment Action
Checking parts 100% visually for hole block
 
3. Process Flow
Process Flow Description
1)Cutting 2)Draw 3)Head Formation 4)Punching 5)Rough Grinding 6)CNC Head Turning 7)CNC Boring & Facing 8)Tapping 9)Chamfering 10)Final Grinding 11)Final Inspection 12)Oiling 13)Packing & Dispatch
 
4. Process Details
Process / Operation Punching
Outsource No
Machine / Cell Power Press
Machine / Cell No. Punching Deptt
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MethodSkip during inspectionAfter verification it was observed that parts was skipped during inspection .X
MaterialWrong grade material usedAfter verification we found material grade as per std.O
MethodOperation Miss part mixedAfter verification we found there was no chance of mixingO
ToolPunch damageAfter verification we found punch was damage during running operation.X
MachineDF punch stroke length lessIt was observed that this is no linkage with the defectO
 
6. Inspection Method Analysis (Current)
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size 2X Smp std
7. Root Cause Analysis (Occurance)
Why 1 Tension hole block found .
Why 2 punch burr/chips was generated in the tension hole
Why 3 tension punch was damaged during in process.
Why 4 Punch setting was loosed
Why 5
Root Cause (Occurance) Punch setting was loosed
 
Root Cause Analysis (Outflow)
Why 1 Tension hole block found .
Why 2 Could not be detected at final inspection
Why 3 Skipped in Sampling inspection
Why 4
Why 5
Root Cause (Outflow) Skipped in Sampling inspection
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceTraining will be provided to Satter to check the settings after installing the punch and die on the machine.Mr. Paramjit25/06/202425/06/2024Completed
OccuranceThe condition of the punch and die should be checked by the setter every hour.Mr. Rajinder26/06/202425/06/2024Completed
OccuranceQ-alert to be displayed at the Punching station.Mr. Princ24/06/202422/06/2024Completed
Outflow100% inspection to be start at final inspection by pin plug gauge.Mr. Ankush25/06/202424/06/2024Completed
OutflowQ-alert to be displayed at the Final station.Mr. Princ24/06/202422/06/2024Completed
OccurancePunching WI to be updatedMr. Princ26/06/202425/06/2024Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details 100% inspection start with pin plug gauge
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
10. Evidance of Countermeasure
Occurance (Before) Die frequently monitoring checkpoint was not available in the WI.
876_Occurance_Before.jpg
Occurance (After) The condition of the punch and die should be checked by the setter every hour. this point to be added in WI.
876_Occurance_After.jpg
Outflow (Before) Sampling plan followed
876_Outflow_Before.jpg
Outflow (After) Q-alert to be displayed and 100 % inspection to be started at final Q-gate.
876_Outflow_After.jpg
 
11. Horizontal Deployment
Horizontal Deployment Required No
Applicable Machine / Model / Plant K-86
 
12. Document Review
Documents ControlPlan, PMCheckSheet, PFMEA, WISOP
Specify Other Document No
 
13. Effectiveness Of Action
Reviewed Quantity 20000
Reason for submission Reviewed next 3 lots found ok