QFR No - 8000879489
Defect Details
NC No. 8000879489
NC Date 22/06/2024
NC Submission Date
Part No. F1LG00902B
Part Name SEAT PIPE -K86A
Supplier Name & Code 100538-NARINDER PARKASH AND CO
ETL Plant 1146-ETL Suspension Narasapura
Defect Details HIGHT O/SIZE.-TOTAL LENGTH MORE
 
1. Problem Description
Defect Description K86 SEAT PIPE TOTAL LENGTH MORE ISSUE
Detection Stage Inprocess
Problem Severity Fitment
NG Quantity 3
Is Defect Repeatative? Yes
Defect Sketch / Photo i2z4kjrrzalkbmbwopa4sgmv.gif
Supplier Communication Details
Quality Head Email ID quality@npcindustries.in
Plant Head/CEO Email ID anand@npcindustries.in
MD Email ID ajay@npcindustries.in
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
3000
9600
0
1500
0
14100
Check Qty
3000
9600
0
0
0
12600
NG Qty
200
0
0
0
0
200
 
Scrap 0
Rework 200
Under Deviation 0
Containment Action
100% visual inspection for model mix
 
3. Process Flow
Process Flow Description
1)Cutting 2)Draw 3)Head Formation 4)Punching 5)Rough Grinding 6)CNC Head Turning 7)CNC Boring & Facing 8)Tapping 9)Chamfering 10)Final Grinding 11)Final Inspection 12)Cleaning 13)Oiling 14)Packing & Dispatch
 
4. Process Details
Process / Operation Packing
Outsource No
Machine / Cell Packing
Machine / Cell No. Packing Deptt
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MethodWrong identification tagAfter verification we found correct identification tag foundO
ManQuality Inspector NegligenceVerified and found OK. No linkage with defectO
MethodMaterial mix-up during transit form one station to another station.After verification we found material was not mixed during transitO
ManPacking persons were untrainedAfter verification we found packing persons were trainedO
MethodPacking Method InadequateAfter verification we found packing method was inadequate for prevent the mixup.X
 
6. Inspection Method Analysis (Current)
Inspection Method Other
Other Inspection Method Visual
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100 %
7. Root Cause Analysis (Occurance)
Why 1 Total length variation found in seatpipe .
Why 2 Other model mix-up found with K86 seat pipe.
Why 3 Other model was mixed during the packing stage.
Why 4 Other model pieces were remaining in the oil tray during packing.
Why 5 All pieces from the oiled holding tray bin were directly emptied onto the tray at one time.
Root Cause (Occurance) All pieces from the oiled holding tray bin were directly emptied onto the tray at one time.
 
Root Cause Analysis (Outflow)
Why 1 Total length variation found in seatpipe .
Why 2 Other model mix-up could not be detected .
Why 3 Other model mixed at packing station after final inspection .
Why 4 No checkpoint is available at packing station.
Why 5
Root Cause (Outflow) No checkpoint is available at packing station.
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceParts should be picked for packing directly from the Oiling holding tray.Mr. Ankush29/06/202424/06/2024Completed
OutflowThe Packing Work Instruction (WI) should be updated, implemented, and followed.Mr. Vinay27/06/202425/06/2024Completed
OccuranceQ-alert to be displayed at packing station.Mr. Princ23/07/202422/06/2024Completed
OutflowInspection of 5 pieces for model mix-up starts every hour at the packing stage.Mr. Ankush25/07/202424/06/2024Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details New inspection check point added at packing stage
Inspection Method Other
Other Inspection Method Visual
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size 5 pcs/ Hr
10. Evidance of Countermeasure
Occurance (Before) All pieces from the oiled holding tray bin were directly emptied onto the tray at one time.
877_Occurance_Before.jpeg
Occurance (After) Parts should be picked for packing directly from the Oiling holding tray.
877_Occurance_After.jpeg
Outflow (Before) No checkpoint is available at packing station.
877_Outflow_Before.jpg
Outflow (After) The Packing Work Instruction (WI) should be updated, implemented, and followed and inspection checkpoint no. 5 updated.
877_Outflow_After.jpg
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant all similar model
 
12. Document Review
Documents ControlPlan, PFMEA, WISOP
Specify Other Document no
 
13. Effectiveness Of Action
Reviewed Quantity 20000
Reason for submission Reviewed next three lots found ok