QFR No - 8000880024
Defect Details
NC No. | 8000880024 |
NC Date | 26/06/2024 |
NC Submission Date | |
Part No. | 080FA04433 |
Part Name | FORK PIPE MACHINED - CT100 |
Supplier Name & Code | 101223-SANGKAJ BRIGHT WIRES PRIVATE L |
ETL Plant | 1146-ETL Suspension Narasapura |
Defect Details | THREADING NOT OK- |
1. Problem Description
Defect Description | CT 100 FORK PIPE MACHINED THREADING ISSUE (THREAD PLUG GAUGE GO NOT QUALIFY ) |
Detection Stage | Inprocess |
Problem Severity | Fitment |
NG Quantity | 165 |
Is Defect Repeatative? | No |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | mayursurese11@gmail.com |
Plant Head/CEO Email ID | steel@sangkaj.com |
MD Email ID | anirudh.2007@hotmail.com |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
0
|
0
|
0
|
2000
|
1000
|
3000
|
Check Qty |
0
|
0
|
0
|
2000
|
1000
|
3000
|
NG Qty |
0
|
0
|
0
|
1
|
0
|
1
|
Scrap | 0 |
Rework | 1 |
Under Deviation | 0 |
Containment Action |
---|
LAST 2 YEARS PROCESS REJECTION GIVEN BY K228 |
3. Process Flow
Process Flow Description |
---|
Cnc 1st-Cnc 2nd-Drill-Final Inspection -Dispatch |
4. Process Details
Process / Operation | CNC 1ST SIDE |
Outsource | No |
Machine / Cell | MACHINE |
Machine / Cell No. | 1,2,3,4,5 |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Machine | M26X1P-6H Gauge not pass | Wrong offset given by operator | O |
6. Inspection Method Analysis (Current)
Inspection Method | Gauge |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | Sampling |
Sampling | No |
Sample Size | 5nos |
7. Root Cause Analysis (Occurance)
Why 1 | M2X1P-6H Gauge not answered |
Why 2 | Insert wear out |
Why 3 | After changing new insert At The Time of correction operator taken 0.3mm offset instead of 0.03mm. |
Why 4 | Wrong offset given by operators. |
Why 5 | Wear offset not lock in programm |
Root Cause (Occurance) | Wear offset not lock in programm |
Root Cause Analysis (Outflow)
Why 1 | M26X1P-6H Thread not answered |
Why 2 | Inspection as a sampling basis |
Why 3 | Inspection Done On Sampling Basis. (5 Nos / Lot) |
Why 4 | |
Why 5 | |
Root Cause (Outflow) | Inspection Done On Sampling Basis. (5 Nos / Lot) |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Occurance | Wear Offset locked By 0.03mm In CNC Machine. | Mayur | 28/06/2024 | 29/06/2024 | Completed |
Outflow | Started 100% Inspection At Machining Stage With The Help Of TPG GO and NOGO. | Pratap Behra | 28/06/2024 | 29/06/2024 | Completed |
Occurance | Too life decided & Lock in CNC Machine. | Mayur | 28/06/2024 | 29/06/2024 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | No |
Change Details | 100% inspection at CNC Stage |
Inspection Method | Gauge |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | Sampling |
Sampling | No |
Sample Size | 50 |
10. Evidance of Countermeasure
Occurance (Before) |
NO INTERLOCK CNC MC 893_Occurance_Before.jpg |
Occurance (After) |
0.03 mm interlock 893_Occurance_After.png |
Outflow (Before) |
Sampling basis inspection 893_Outflow_Before.png |
Outflow (After) |
Sampling basic inspection but 50 nos check every lot & OPL dispalyed FID 893_Outflow_After.png |
11. Horizontal Deployment
Horizontal Deployment Required | Yes |
Applicable Machine / Model / Plant | K3 FORK PIPE,K17 FORK PIPE,ATHER,Ampere |
12. Document Review
Documents | WISOP, InspCheckSheet |
Specify Other Document | OPL |
13. Effectiveness Of Action
Reviewed Quantity | 2000 |
Reason for submission | Reviewed next two lots found ok |