QFR No - 8000880024
Defect Details
NC No. 8000880024
NC Date 26/06/2024
NC Submission Date
Part No. 080FA04433
Part Name FORK PIPE MACHINED - CT100
Supplier Name & Code 101223-SANGKAJ BRIGHT WIRES PRIVATE L
ETL Plant 1146-ETL Suspension Narasapura
Defect Details THREADING NOT OK-
 
1. Problem Description
Defect Description CT 100 FORK PIPE MACHINED THREADING ISSUE (THREAD PLUG GAUGE GO NOT QUALIFY )
Detection Stage Inprocess
Problem Severity Fitment
NG Quantity 165
Is Defect Repeatative? No
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID mayursurese11@gmail.com
Plant Head/CEO Email ID steel@sangkaj.com
MD Email ID anirudh.2007@hotmail.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
0
0
0
2000
1000
3000
Check Qty
0
0
0
2000
1000
3000
NG Qty
0
0
0
1
0
1
 
Scrap 0
Rework 1
Under Deviation 0
Containment Action
LAST 2 YEARS PROCESS REJECTION GIVEN BY K228
 
3. Process Flow
Process Flow Description
Cnc 1st-Cnc 2nd-Drill-Final Inspection -Dispatch
 
4. Process Details
Process / Operation CNC 1ST SIDE
Outsource No
Machine / Cell MACHINE
Machine / Cell No. 1,2,3,4,5
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MachineM26X1P-6H Gauge not passWrong offset given by operatorO
 
6. Inspection Method Analysis (Current)
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size 5nos
7. Root Cause Analysis (Occurance)
Why 1 M2X1P-6H Gauge not answered
Why 2 Insert wear out
Why 3 After changing new insert At The Time of correction operator taken 0.3mm offset instead of 0.03mm.
Why 4 Wrong offset given by operators.
Why 5 Wear offset not lock in programm
Root Cause (Occurance) Wear offset not lock in programm
 
Root Cause Analysis (Outflow)
Why 1 M26X1P-6H Thread not answered
Why 2 Inspection as a sampling basis
Why 3 Inspection Done On Sampling Basis. (5 Nos / Lot)
Why 4
Why 5
Root Cause (Outflow) Inspection Done On Sampling Basis. (5 Nos / Lot)
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceWear Offset locked By 0.03mm In CNC Machine.Mayur28/06/202429/06/2024Completed
OutflowStarted 100% Inspection At Machining Stage With The Help Of TPG GO and NOGO.Pratap Behra28/06/202429/06/2024Completed
OccuranceToo life decided & Lock in CNC Machine.Mayur28/06/202429/06/2024Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System No
Change Details 100% inspection at CNC Stage
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size 50
10. Evidance of Countermeasure
Occurance (Before) NO INTERLOCK CNC MC
893_Occurance_Before.jpg
Occurance (After) 0.03 mm interlock
893_Occurance_After.png
Outflow (Before) Sampling basis inspection
893_Outflow_Before.png
Outflow (After) Sampling basic inspection but 50 nos check every lot & OPL dispalyed FID
893_Outflow_After.png
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant K3 FORK PIPE,K17 FORK PIPE,ATHER,Ampere
 
12. Document Review
Documents WISOP, InspCheckSheet
Specify Other Document OPL
 
13. Effectiveness Of Action
Reviewed Quantity 2000
Reason for submission Reviewed next two lots found ok