QFR No - 8000880725
Defect Details
NC No. | 8000880725 |
NC Date | 02/07/2024 |
NC Submission Date | |
Part No. | F2FA10933M |
Part Name | FORK PIPE MACHINED - J1A |
Supplier Name & Code | 101030-TUBE INVESTMENTS OF INDIA LTD |
ETL Plant | 1117-ETL K-228/9 Suspension |
Defect Details | NOT AS PER SPECIFICATION-SHORT LENGTH |
1. Problem Description
Defect Description | SHORT LENGTH |
Detection Stage | Inprocess |
Problem Severity | Fitment |
NG Quantity | 12 |
Is Defect Repeatative? | Yes |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | AmitVD@tii.murugappa.com |
Plant Head/CEO Email ID | guptaajay@tii.murugappa.com |
MD Email ID | mukeshahuja@tii.murugappa.com |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
2000
|
0
|
0
|
0
|
1500
|
3500
|
Check Qty |
2000
|
0
|
0
|
0
|
1500
|
3500
|
NG Qty |
12
|
0
|
0
|
0
|
12
|
24
|
Scrap | 12 |
Rework | 0 |
Under Deviation | 0 |
Containment Action |
---|
All Stock available at ETL end & Inhouse checked for the Threading Parameter |
3. Process Flow
Process Flow Description |
---|
Raw Material Inspection- Machining (Cualking & Threading)-Drilling-Oiling-Final Inspection-Dispatch |
4. Process Details
Process / Operation | Machining |
Outsource | No |
Machine / Cell | CNC Machine Cell |
Machine / Cell No. | Machine No.22/23 &14 |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Method | No Inspection for Length Parameter | Inspection on the Sampling Basis | X |
Machine | Stopper Condtion Not OK | The uneven resting surface of the stopper | X |
6. Inspection Method Analysis (Current)
Inspection Method | Instrument |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | Sampling |
Sampling | No |
Sample Size | Sampling |
7. Root Cause Analysis (Occurance)
Why 1 | Total Length Observed Undersize |
Why 2 | Tube end face not resting properly on Stopper Surface |
Why 3 | The uneven resting surface of the stopper |
Why 4 | During Mass production resting surface of the stopper wears out |
Why 5 | The current Stopper, material used was MS & Not enough which caused the stopper wear out |
Root Cause (Occurance) | The current Stopper, material used was MS & Not enough which caused the stopper wear out |
Root Cause Analysis (Outflow)
Why 1 | Not Detected during the Final Inspection & PDIR Why 2 |
Why 2 | Inspection on the Sampling Basis |
Why 3 | No Length Inspection gauge is available for the 100 % Inspection |
Why 4 | |
Why 5 | |
Root Cause (Outflow) | No Length Inspection gauge is available for the 100 % Inspection |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Occurance | The Carbide material was used for the new stopper & made Properly hard ?50 to 65 HB ? & to prevent loose burr from sticking to the stopper, Also Provision was made for the coolant to come out from the stopper. | Mr. Rathod KS | 03/07/2024 | 03/07/2024 | Completed |
Outflow | Length Gauge added for the 100% Inspection | Mr. Dethe SS | 03/07/2024 | 03/07/2024 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | Yes |
Change Details | Length Inspection Gauge Added for the 100 % Inspection |
Inspection Method | Gauge |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100 % |
10. Evidance of Countermeasure
Occurance (Before) |
The current Stopper, material used was MS & Not enough which caused the stopper to wear out 901_Occurance_Before.pdf |
Occurance (After) |
The Carbide material was used for the new stopper & made Properly hard ?50 to 65 HB ? & to prevent loose burr from sticking
to the stopper, Also Provision was made for the coolant to come out from the stopper. 901_Occurance_After.pdf |
Outflow (Before) |
Before: No 100 % Inspection on Length Gauge 901_Outflow_Before.pdf |
Outflow (After) |
After: 100 % Inspection Started by Using Length Inspection Gauge 901_Outflow_After.pdf |
11. Horizontal Deployment
Horizontal Deployment Required | Yes |
Applicable Machine / Model / Plant | All Model |
12. Document Review
Documents | WISOP, InspCheckSheet |
Specify Other Document | WI |
13. Effectiveness Of Action
Reviewed Quantity | 120 |
Reason for submission | Ok |