QFR No - 8000880725
Defect Details
NC No. 8000880725
NC Date 02/07/2024
NC Submission Date
Part No. F2FA10933M
Part Name FORK PIPE MACHINED - J1A
Supplier Name & Code 101030-TUBE INVESTMENTS OF INDIA LTD
ETL Plant 1117-ETL K-228/9 Suspension
Defect Details NOT AS PER SPECIFICATION-SHORT LENGTH
 
1. Problem Description
Defect Description SHORT LENGTH
Detection Stage Inprocess
Problem Severity Fitment
NG Quantity 12
Is Defect Repeatative? Yes
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID AmitVD@tii.murugappa.com
Plant Head/CEO Email ID guptaajay@tii.murugappa.com
MD Email ID mukeshahuja@tii.murugappa.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
2000
0
0
0
1500
3500
Check Qty
2000
0
0
0
1500
3500
NG Qty
12
0
0
0
12
24
 
Scrap 12
Rework 0
Under Deviation 0
Containment Action
All Stock available at ETL end & Inhouse checked for the Threading Parameter
 
3. Process Flow
Process Flow Description
Raw Material Inspection- Machining (Cualking & Threading)-Drilling-Oiling-Final Inspection-Dispatch
 
4. Process Details
Process / Operation Machining
Outsource No
Machine / Cell CNC Machine Cell
Machine / Cell No. Machine No.22/23 &14
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MethodNo Inspection for Length ParameterInspection on the Sampling BasisX
MachineStopper Condtion Not OKThe uneven resting surface of the stopperX
 
6. Inspection Method Analysis (Current)
Inspection Method Instrument
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size Sampling
7. Root Cause Analysis (Occurance)
Why 1 Total Length Observed Undersize
Why 2 Tube end face not resting properly on Stopper Surface
Why 3 The uneven resting surface of the stopper
Why 4 During Mass production resting surface of the stopper wears out
Why 5 The current Stopper, material used was MS & Not enough which caused the stopper wear out
Root Cause (Occurance) The current Stopper, material used was MS & Not enough which caused the stopper wear out
 
Root Cause Analysis (Outflow)
Why 1 Not Detected during the Final Inspection & PDIR Why 2
Why 2 Inspection on the Sampling Basis
Why 3 No Length Inspection gauge is available for the 100 % Inspection
Why 4
Why 5
Root Cause (Outflow) No Length Inspection gauge is available for the 100 % Inspection
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceThe Carbide material was used for the new stopper & made Properly hard ?50 to 65 HB ? & to prevent loose burr from sticking to the stopper, Also Provision was made for the coolant to come out from the stopper.Mr. Rathod KS03/07/202403/07/2024Completed
OutflowLength Gauge added for the 100% InspectionMr. Dethe SS03/07/202403/07/2024Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details Length Inspection Gauge Added for the 100 % Inspection
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100 %
10. Evidance of Countermeasure
Occurance (Before) The current Stopper, material used was MS & Not enough which caused the stopper to wear out
901_Occurance_Before.pdf
Occurance (After) The Carbide material was used for the new stopper & made Properly hard ?50 to 65 HB ? & to prevent loose burr from sticking to the stopper, Also Provision was made for the coolant to come out from the stopper.
901_Occurance_After.pdf
Outflow (Before) Before: No 100 % Inspection on Length Gauge
901_Outflow_Before.pdf
Outflow (After) After: 100 % Inspection Started by Using Length Inspection Gauge
901_Outflow_After.pdf
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant All Model
 
12. Document Review
Documents WISOP, InspCheckSheet
Specify Other Document WI
 
13. Effectiveness Of Action
Reviewed Quantity 120
Reason for submission Ok