QFR No - 8000881721
Defect Details
NC No. | 8000881721 |
NC Date | 08/07/2024 |
NC Submission Date | |
Part No. | F2DZ00912O |
Part Name | FORK BOLT - K8 |
Supplier Name & Code | 101263-SINGLA PRECISION SCREWS |
ETL Plant | 1117-ETL K-228/9 Suspension |
Defect Details | NOT AS PER SPECIFICATION-OD |
1. Problem Description
Defect Description | OD oversize |
Detection Stage | Inprocess |
Problem Severity | Fitment |
NG Quantity | 22 |
Is Defect Repeatative? | Yes |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | quality@singlaprecision.com |
Plant Head/CEO Email ID | quality@singlaprecision.com |
MD Email ID | aditya@singlaprecision.com |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
540
|
0
|
0
|
2000
|
2000
|
4540
|
Check Qty |
540
|
0
|
0
|
2000
|
2000
|
4540
|
NG Qty |
22
|
0
|
0
|
0
|
0
|
22
|
Scrap | 22 |
Rework | 0 |
Under Deviation | 0 |
Containment Action |
---|
We checked 100% material lying at various stage |
3. Process Flow
Process Flow Description |
---|
1-Raw Material 2-Part Off 3-Punching 4-Drilling + Counter 5-Tapping 6-CNC Turning 7-Rolling 8-Re -Tapping 9-Finish 10-Fiinal Inspection 11-Packing |
4. Process Details
Process / Operation | Punching |
Outsource | No |
Machine / Cell | Punching |
Machine / Cell No. | P-Machine -01 |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Machine | Material to swell in Punching process | Validation And Found NG | X |
Man | UNAWARENESS OF OPERATOR | VALIDATION AND FOUND OPERATOR SKILL LEVEL OK | O |
Material | RM GRADE AND SIZE NOT OK | VALIDATION AND FOUND OK | O |
Tool | Tool may wear | Validated and found ok | O |
Method | Inspection Plan Not Effective | Sampling plan for forging has been Not revised | X |
6. Inspection Method Analysis (Current)
Inspection Method | Instrument |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | Sampling |
Sampling | No |
Sample Size | as per pla |
7. Root Cause Analysis (Occurance)
Why 1 | NOT AS PER SPECIFICATION-OD |
Why 2 | Material to swell in Punching process |
Why 3 | After Punching Process not CLG Process Add |
Why 4 | |
Why 5 | |
Root Cause (Occurance) | CLG operation not add after Punching process |
Root Cause Analysis (Outflow)
Why 1 | NOT AS PER SPECIFICATION-OD |
Why 2 | Inspection Plan was not Effective |
Why 3 | Final inspection standard checking Frequency change 100% Gauge implements |
Why 4 | As per sampling Plan part checking in final inspection |
Why 5 | Ng part skipped from inspection and machine |
Root Cause (Outflow) | Final inspection standard checking Frequency change 100% Gauge implements |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Occurance | Process Drg Add CLG Operation After Punching Process | Mr Ganesh Maurya | 31/07/2024 | 02/08/2024 | Completed |
Outflow | final inspection standard checking Frequency change 100% Gauge implements | Mr Ganesh Maurya | 31/07/2024 | 02/08/2024 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | Yes |
Change Details | Final inspection standard checking Frequency change 100% Gauge implements |
Inspection Method | Gauge |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100 |
10. Evidance of Countermeasure
Occurance (Before) |
CLG operation not add after Punching process 926_Occurance_Before.jpeg |
Occurance (After) |
CLG operation add after Punching process 926_Occurance_After.jpeg |
Outflow (Before) |
final inspection standard checking Frequency 10 pcs 926_Outflow_Before.jpeg |
Outflow (After) |
final inspection standard checking Frequency change 100% Gauge implements 926_Outflow_After.jpeg |
11. Horizontal Deployment
Horizontal Deployment Required | No |
Applicable Machine / Model / Plant | clg 01 |
12. Document Review
Documents | Drawing, ProcessFlowChart |
Specify Other Document | no |
13. Effectiveness Of Action
Reviewed Quantity | 50 |
Reason for submission | 5. Problem Analysis - Need all 4M |