QFR No - 8000881725
Defect Details
NC No. | 8000881725 |
NC Date | 08/07/2024 |
NC Submission Date | |
Part No. | F2LG07102B |
Part Name | SEAT PIPE - J1D |
Supplier Name & Code | 101222-SANGKAJ ENGINEERING PVT LTD- U |
ETL Plant | 1117-ETL K-228/9 Suspension |
Defect Details | THREADING MISSING-WITHOUT THREADING |
1. Problem Description
Defect Description | Thread missing |
Detection Stage | Inprocess |
Problem Severity | Fitment |
NG Quantity | 1 |
Is Defect Repeatative? | Yes |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | aslam@sangkaj.com |
Plant Head/CEO Email ID | steel@sangkaj.com |
MD Email ID | anirudh.2007@hotmail.com |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
1000
|
0
|
0
|
500
|
500
|
2000
|
Check Qty |
1000
|
0
|
0
|
500
|
500
|
2000
|
NG Qty |
1
|
0
|
0
|
0
|
0
|
1
|
Scrap | 1 |
Rework | 0 |
Under Deviation | 0 |
Containment Action |
---|
Segregation of pipeline material, FG material, and Customer end |
3. Process Flow
Process Flow Description |
---|
10.RM Inspection; 20.Parting off and chamfering; 30.Weighing and moly powder application; 40.Draw forging; 50.Head Forging; 60.Rough Grinding; 70A. Collar Machining; 70B. Total length facing, Drilling & Tapping; 80.Hole piercing; 90 DF and Compression hole chamfering; 100.ID Cleaning & Deburring; 110.Finish Grinding; 120.Ultrasonic Cleaning; 130. Final Inspection; 140.Oiling; 150.Packing and storage. |
4. Process Details
Process / Operation | 70B |
Outsource | No |
Machine / Cell | CDL CNC |
Machine / Cell No. | CDL CNC-01 |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Material | Material grade not ok | Material grade found OK. | O |
Man | Machine operator/Final inspector not as per skill materix | Machine operator & Final inspector found as per skill matrix | O |
Tool | Wrong size grade tap used | Tapping tool found ok grade with Ok size | O |
Method | Due to power off Operation not completed | Due to power of Threading operation not completed/missing | X |
Machine | PM not as per plan | PM found as per plan | O |
6. Inspection Method Analysis (Current)
Inspection Method | Other |
Other Inspection Method | Visual |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100 |
7. Root Cause Analysis (Occurance)
Why 1 | Threading missing part produced |
Why 2 | Threading operation not completed |
Why 3 | Programmed on CNC machine for tapping not executed |
Why 4 | Incomplete operation due to power off in running condition. . |
Why 5 | |
Root Cause (Occurance) | Incomplete operation due to power off in running condition. . |
Root Cause Analysis (Outflow)
Why 1 | Threading missing part found at customer end |
Why 2 | Threading missing part not detected/outflows |
Why 3 | Detected part mixup in OK parts |
Why 4 | |
Why 5 | |
Root Cause (Outflow) | Threading missing part outflows due to mixup |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Occurance | In Work instruction add checkpoint for inspection of all parameter after power off. | Mr.Irfan | 07/08/2024 | 06/08/2024 | Completed |
Outflow | Red paint on head side for threading missing / operation missing part (Add in Work instruction ) | Mr.Irfan | 07/08/2024 | 06/08/2024 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | Yes |
Change Details | 100 % inspection with threading side blue color dot. |
Inspection Method | Other |
Other Inspection Method | Visual |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100 |
10. Evidance of Countermeasure
Occurance (Before) |
NO instruction point for machine after power off 922_Occurance_Before.jpg |
Occurance (After) |
Instruction added in Work instruction for Checking all parameters after power off 922_Occurance_After.jpg |
Outflow (Before) |
Operation missing/threading missing part no special treatment 922_Outflow_Before.jpg |
Outflow (After) |
Red spray paint apply on head for operation missing/thread missing part instruction added in WI 922_Outflow_After.jpg |
11. Horizontal Deployment
Horizontal Deployment Required | No |
Applicable Machine / Model / Plant | NA |
12. Document Review
Documents | WISOP |
Specify Other Document | No |
13. Effectiveness Of Action
Reviewed Quantity | 50 |
Reason for submission | ok |