QFR No - 8000882493
Defect Details
NC No. 8000882493
NC Date 14/07/2024
NC Submission Date
Part No. F2FA10933M
Part Name FORK PIPE MACHINED - J1A
Supplier Name & Code 100576-SANGKAJ BRIGHT WIRES PVT LTD
ETL Plant 1117-ETL K-228/9 Suspension
Defect Details NOT AS PER SPECIFICATION-DU BUSH OD O/S
 
1. Problem Description
Defect Description DU BUSH OD O/S
Detection Stage Inprocess
Problem Severity Fitment
NG Quantity 53
Is Defect Repeatative? Yes
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID brightwire.qa@sangkaj.com
Plant Head/CEO Email ID steel@sangkaj.com
MD Email ID anirudh.2007@hotmail.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
3500
0
0
2500
1500
7500
Check Qty
3500
0
0
2500
1500
7500
NG Qty
53
0
0
0
0
53
 
Scrap 53
Rework 0
Under Deviation 0
Containment Action
1) At ETL end verified 3500 Nos & 53 nos found not ok. 2) At SBWPL end verify 4000 nos & all part found ok. 3) For ok parts provided 100 % Verification identification marking on DU bush OD.
 
3. Process Flow
Process Flow Description
Receipt Of Material - Inward Inspection - CNC 1st Setup - CNC 2nd Setup - Drilling - Final Inspection - Air Cleaning - Dispatch
 
4. Process Details
Process / Operation CNC 2nd Setup
Outsource No
Machine / Cell Machining
Machine / Cell No. Fork Pipe Machining
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MaterialMaterial Hardness not okVerified found okO
MachineWear Offset lockVerified found not okX
MethodLoading & UnloadingVerified Found OKO
ManOperator NewVerified found not okX
ToolTool holder looseVerified Found OkO
MachineSpindle Run outVerified found okO
 
6. Inspection Method Analysis (Current)
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size 10 nos
7. Root Cause Analysis (Occurance)
Why 1 DU Bush OD Oversize
Why 2 DU Bush OD At lower side
Why 3 At the time of correction operator take offset 0.04. reading get higher size by 0.01
Why 4 Wrong offset given by operator
Why 5 Wear offset not lock in cnc machine in 0.05mm
Root Cause (Occurance) Wear offset not lock in cnc machine in 0.05mm
 
Root Cause Analysis (Outflow)
Why 1 DU Bush OD Oversize
Why 2 inspection skipped by Operator
Why 3 inspection done on sampling basis.
Why 4
Why 5
Root Cause (Outflow) inspection done on sampling basis.
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
Outflow`For ok parts provided 100 % Verification identification marking on DU Bush OD.Mr. Nitin Puri14/07/202414/07/2024Completed
OccuranceProvide On job Training and awareness given to all inspectors and CNC Operator for DU Bush OD oversize & its importanceMr. Barik & Nitin Puri14/07/202414/07/2024Completed
OccuranceWear Offset lock by 0.03mmMr. Barik15/07/202415/07/2024Completed
OutflowDisplay the OPLMr. Mukesh Rathod & Manoj Pathe14/07/202414/07/2024Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details started 100% Inspection at final inspection stage only for 10 days. after 10 days we have started the sampling basis inspection.
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
10. Evidance of Countermeasure
Occurance (Before) Wear Offset lock in 0.05mm
936_Occurance_Before.jpg
Occurance (After) Wear Offset lock in 0.01mm
936_Occurance_After.jpg
Outflow (Before) Identification not provided after inspection
936_Outflow_Before.jpg
Outflow (After) Identification mark provided after inspection
936_Outflow_After.xlsx
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant All model
 
12. Document Review
Documents WISOP
Specify Other Document OPL
 
13. Effectiveness Of Action
Reviewed Quantity 144
Reason for submission Why Wear offset not consider 0.010mm In future it will repeat So reverify for wear offset 0.010mm against 0.03mm