QFR No - 8000882627
Defect Details
NC No. 8000882627
NC Date 15/07/2024
NC Submission Date
Part No. F2FA16633M
Part Name FORK PIPE MACHINED - K17B/D
Supplier Name & Code 101030-TUBE INVESTMENTS OF INDIA LTD
ETL Plant 1117-ETL K-228/9 Suspension
Defect Details NOT AS PER SPECIFICATION-THREADING NG
 
1. Problem Description
Defect Description THREADING NG (No go Qualify)
Detection Stage Receipt
Problem Severity Fitment
NG Quantity 3
Is Defect Repeatative? Yes
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID AmitVD@tii.murugappa.com
Plant Head/CEO Email ID guptaajay@tii.murugappa.com
MD Email ID mukeshahuja@tii.murugappa.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
500
0
0
0
0
500
Check Qty
500
0
0
0
0
500
NG Qty
3
0
0
0
0
3
 
Scrap 3
Rework 0
Under Deviation 0
Containment Action
All Stock available at ETL end & Inhouse checked for the Threading Parameter
 
3. Process Flow
Process Flow Description
Raw Material Inspection- Machining (Cualking & Threading)-Drilling-Oiling-Final Inspection-Dispatch
 
4. Process Details
Process / Operation Machining
Outsource No
Machine / Cell CNC Machine Cell
Machine / Cell No. Machine No:22 & 23
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MethodNo step wise offset given & verified it`s impact to achieve the product characteristicsWrong off set at time of set upX
MethodInspection on a sampling basisInspection on a sampling basis which is not adequate for detectionX
 
6. Inspection Method Analysis (Current)
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size 13 Nos/500
7. Root Cause Analysis (Occurance)
Why 1 Threading NG - Threading Minor Dia observed under size.
Why 2 Excess Material removal during machining Cut for threading Minor Dia
Why 3 During the Machining setup geometric parameter setting not proper
Why 4 The wrong offset value was put during the setup.
Why 5 The CNC Program did not have Offest value interlocking to give threading offset. & hence offset could be given from 10 microns to 0.2 mm.
Root Cause (Occurance) The CNC Program did not have Offest value interlocking to give threading offset. & hence offset could be given from 10 microns to 0.2 mm.
 
Root Cause Analysis (Outflow)
Why 1 Not detected during the final inspection
Why 2 Inspection on a sampling basis which is not adequate for detection
Why 3
Why 4
Why 5
Root Cause (Outflow) Inspection on a sampling basis which is not adequate for detection
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceThreading Offset Value has been locked in the CNC Program for 50 microns so that more than 50 micron offset cannot be given.Mr. Rathod KS16/07/202416/07/2024Completed
OutflowSampling Inspection Qty. Doubled from 13 Nos/500 Nos. . to 26 Nos./500 Nos.Mr. Dethe SS16/07/202416/07/2024Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details Sampling Inspection Qty. Doubled from 13 Nos/500 Nos. to 26 Nos./500 Nos.
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size 26/500 Nos
10. Evidance of Countermeasure
Occurance (Before) Before: The CNC Program did not have Offset value interlocking to give threading offset. & hence offset could be given from 10 microns to 0.2 mm.
934_Occurance_Before.pdf
Occurance (After) After: Threading Offset Value has been locked in the CNC Program for 50 microns so that more than 50-micron offset cannot be given.
934_Occurance_After.pdf
Outflow (Before) Sampling Inspection Qty. 13 Nos/500 Nos. Not Adhequete
934_Outflow_Before.pdf
Outflow (After) Sampling Inspection Qty. Doubled from 13 Nos/500 Nos. . to 26 Nos./500 Nos
934_Outflow_After.pdf
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant All Models
 
12. Document Review
Documents WISOP, InspCheckSheet
Specify Other Document WI
 
13. Effectiveness Of Action
Reviewed Quantity 111
Reason for submission ok