QFR No - 8000882706
Defect Details
NC No. 8000882706
NC Date 17/07/2024
NC Submission Date
Part No. F2DZ04512B
Part Name SCREW CAP/FORK BOLT ABWA ADJUSTABLE
Supplier Name & Code 100106-SHARP ENGINEERS.
ETL Plant 1118-ETL E-92,93 Suspension
Defect Details DIMETER UNDERSIZE-7+0.1 UINDER SIZE
 
1. Problem Description
Defect Description 7+0.1 dimension found under size by up to 0.2 mm
Detection Stage Receipt
Problem Severity Fitment
NG Quantity 118
Is Defect Repeatative? No
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID quality@sharp-engineers.com
Plant Head/CEO Email ID kurund.ma@sharp-engineers.com
MD Email ID urkhandelwal@sharp-engineers.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
450
0
0
1200
0
1650
Check Qty
450
0
0
1200
0
1650
NG Qty
118
0
0
28
0
146
 
Scrap 146
Rework 0
Under Deviation 0
Containment Action
Pipline material segregated at Customer and our end
 
3. Process Flow
Process Flow Description
RM incoming Inspection
 
4. Process Details
Process / Operation CNC
Outsource No
Machine / Cell CNC
Machine / Cell No. CNC
5. Problem Analysis
Type Possible Cause Fact Verification Jud
ToolInsert brokenNo insert brokenO
MethodFixture not clesn properlyFixture cleaned after every cycle regardi ng Work Instruction also displayed at Machine stageO
ManNew manpowerManpower available as per skill matrixO
ManUnskill operatorSkill operator availableO
ManWrong setting done by operatorSetting done ok, also Setup approval report evidentO
Machinepower cutno power cutO
ToolInsert wear outNo insert wear outO
MethodInsert not change at defined frequencyAs per tool history card its obeserved tool changed at defined frequencyO
MethodPart not validated after replacement of insertPart not validated after replacement of insertX
ToolTool ChangeNo any tool changedO
MaterialRM changeRM found as pr requirementO
MachineMachine changedNo machine changeO
 
6. Inspection Method Analysis (Current)
Inspection Method Instrument
Other Inspection Method
Check Point at Final Inspection No
Checking Freq. Sampling
Sampling No
Sample Size 5 nos
7. Root Cause Analysis (Occurance)
Why 1 Dimension 7 undersized
Why 2 Dimension 7 +0.2/+0.1 observed 6.95
Why 3 Insert changed
Why 4 Insert life over
Why 5 verification not done after replacement of insert coz dependency on operator.
Root Cause (Occurance) Part not validated after replacement of insert by operator
 
Root Cause Analysis (Outflow)
Why 1 Dimension 7 undersized
Why 2 Skip from inspection
Why 3 No checkpoint at final inspection
Why 4
Why 5
Root Cause (Outflow) No checkpoint at final inspection
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OutflowCheckpoint added in Final inspection and verification started at PDI stageOmkar Bhange31/07/202431/07/2024Completed
OutflowPart verification started by Supervisor and Inprocess engineer after replacement of Insert.Ingole and Yogesh chavan30/07/202431/07/2024Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details Verification started by Supervisor and Inprocess engineer
Inspection Method Instrument
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size 5
10. Evidance of Countermeasure
Occurance (Before) Operator dependency for part verification after replacement of insert
944_Occurance_Before.jpg
Occurance (After) On job training given to Production supervisor and Inprocess engineer for verification of part after replacement of insert
944_Occurance_After.jpeg
Outflow (Before) No check point in final inspection
944_Outflow_Before.jpg
Outflow (After) Check point added in Final inspection also verification point added in PDI report
944_Outflow_After.jpg
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant For all machine
 
12. Document Review
Documents ControlPlan, PFMEA, WISOP, InspCheckSheet
Specify Other Document NA
 
13. Effectiveness Of Action
Reviewed Quantity 500
Reason for submission after correction issue not observed.