QFR No - 8000884034
Defect Details
NC No. 8000884034
NC Date 25/07/2024
NC Submission Date
Part No. F2FA19033M
Part Name K0PG FORK PIPE MACHINED
Supplier Name & Code 101223-SANGKAJ BRIGHT WIRES PRIVATE L
ETL Plant 1146-ETL Suspension Narasapura
Defect Details EXCESS M/CING-DOUBLE GROOVE OPERATION
 
1. Problem Description
Defect Description K0PG fork pipe ID double groove operation
Detection Stage Inprocess
Problem Severity Fitment
NG Quantity 3
Is Defect Repeatative? Yes
Defect Sketch / Photo l055dbjk0qj0wsubay1neyhu.jpg
Supplier Communication Details
Quality Head Email ID mayursurse11@gmail.com
Plant Head/CEO Email ID steel@sangkaj.com
MD Email ID anirudh.2007@hotmail.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
2000
0
0
1000
1000
4000
Check Qty
1998
0
0
1000
1000
3998
NG Qty
2
0
0
0
0
2
 
Scrap 1
Rework 0
Under Deviation 0
Containment Action
100% check all stock visual
 
3. Process Flow
Process Flow Description
Incoming Raw Material +Inward Inspection Raw Material+ CNC 1st set up+ CNC 2nd set up + Drilling + Air Cleaning + Final Inspection + Movement & PDI Inspection + Dispatch
 
4. Process Details
Process / Operation CNC MACHINING
Outsource No
Machine / Cell CNC CELL
Machine / Cell No. 2
5. Problem Analysis
Type Possible Cause Fact Verification Jud
ManWrong offset given by operator at the time of reworkat time of rework operator could not judge offser 1.5mmO
 
6. Inspection Method Analysis (Current)
Inspection Method Other
Other Inspection Method Visual
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 5nos
7. Root Cause Analysis (Occurance)
Why 1 Doable Groove
Why 2 After changing insert job at lower out of specification
Why 3 End of shift that job rework
Why 4 Offset not given by operator.
Why 5
Root Cause (Occurance) Offset not given by operator.
 
Root Cause Analysis (Outflow)
Why 1 Doable Groove
Why 2 Rejected material mix-up with ok material
Why 3 Rejection bin provided but not daily rejection rework clear
Why 4
Why 5
Root Cause (Outflow) Rejection bin provided but not daily rejection rework clear
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceOffset not given by operator.Supervisor04/08/2024Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System No
Change Details no changes
Inspection Method Other
Other Inspection Method Visual
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 5
10. Evidance of Countermeasure
Occurance (Before) no offset locking
964_Occurance_Before.png
Occurance (After) Offset locking
964_Occurance_After.png
Outflow (Before) rework data not available
964_Outflow_Before.png
Outflow (After) Rej rework & red yellow bin available
964_Outflow_After.png
 
11. Horizontal Deployment
Horizontal Deployment Required No
Applicable Machine / Model / Plant NO MODEL SAME AS
 
12. Document Review
Documents
Specify Other Document One point lesson
 
13. Effectiveness Of Action
Reviewed Quantity 15000
Reason for submission Reviewed next 3 lots found ok no issue