QFR No - 8000884330
Defect Details
NC No. | 8000884330 |
NC Date | 26/07/2024 |
NC Submission Date | |
Part No. | F2AV00302B |
Part Name | BELLOW-B104B |
Supplier Name & Code | 101023-FORES ELASTOMECH INDIA PVT. LT |
ETL Plant | 1117-ETL K-228/9 Suspension |
Defect Details | NOT AS PER SPECIFICATION-CUT MARK , FLOW MARK |
1. Problem Description
Defect Description | Cut mark |
Detection Stage | Inprocess |
Problem Severity | Aesthetic |
NG Quantity | 4 |
Is Defect Repeatative? | Yes |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | malani.pritam@foresgroup.com |
Plant Head/CEO Email ID | singh.barinder@foresgroup.com |
MD Email ID | swamy.pj@foresgroup.com |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
1500
|
0
|
0
|
0
|
0
|
1500
|
Check Qty |
1500
|
0
|
0
|
0
|
0
|
1500
|
NG Qty |
1
|
0
|
0
|
0
|
0
|
1
|
Scrap | 1 |
Rework | 0 |
Under Deviation | 0 |
Containment Action |
---|
Sorted all customer end & Fores end quantity |
3. Process Flow
Process Flow Description |
---|
RM - Mixing- Moulding - Final Inspection - Packing |
4. Process Details
Process / Operation | Moulding |
Outsource | No |
Machine / Cell | Cell no-1 |
Machine / Cell No. | Machine |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Tool | Less material flow in cavity | leakage in mould cavity. | X |
Material | Wrong compound used | Found match with control plan & production report. Checked one month data & found okay | O |
Man | Un skill Inspector | Skill level verified found L3 & Required L3 | O |
Method | Mix up during packing | Offline packing | X |
Machine | Process parameter of moulding not followed | Found matched with control plan & automatic PLC control | O |
6. Inspection Method Analysis (Current)
Inspection Method | Other |
Other Inspection Method | Visual |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100 |
7. Root Cause Analysis (Occurance)
Why 1 | Flow mark |
Why 2 | Less material flow in cavity |
Why 3 | leakage in mould cavity. |
Why 4 | Mould plate parallelism not okay |
Why 5 | |
Root Cause (Occurance) | Mould plate parallelism not okay |
Root Cause Analysis (Outflow)
Why 1 | Flow mark |
Why 2 | Skipped from Fores quality |
Why 3 | Not checked part mixed in okay part after quality inspection |
Why 4 | Offline box packing |
Why 5 | |
Root Cause (Outflow) | Offline box packing |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Occurance | Mould leakage removed by making plate parallelism okay. | Ravi | 11/07/2024 | 26/06/2024 | Completed |
Outflow | `Online packing implemented | Pande | 25/08/2024 | 15/07/2024 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | No |
Change Details | NA |
Inspection Method | Other |
Other Inspection Method | NA |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100 % |
10. Evidance of Countermeasure
Occurance (Before) |
Mould parallelism Not okay 971_Occurance_Before.pdf |
Occurance (After) |
Mould parallelism okay 971_Occurance_After.pdf |
Outflow (Before) |
Offline packing 971_Outflow_Before.jpg |
Outflow (After) |
Online packing 971_Outflow_After.pdf |
11. Horizontal Deployment
Horizontal Deployment Required | Yes |
Applicable Machine / Model / Plant | Cell no 1 |
12. Document Review
Documents | |
Specify Other Document | OPL |
13. Effectiveness Of Action
Reviewed Quantity | 50 |
Reason for submission | OK |