QFR No - 8000884334
Defect Details
NC No. | 8000884334 |
NC Date | 26/07/2024 |
NC Submission Date | |
Part No. | F2CK00403B |
Part Name | CAP NUT XF1C1_1D1 |
Supplier Name & Code | 100106-SHARP ENGINEERS. |
ETL Plant | 1117-ETL K-228/9 Suspension |
Defect Details | DENT MARK-DENT DAMAGE |
1. Problem Description
Defect Description | Hex damage |
Detection Stage | Receipt |
Problem Severity | Function |
NG Quantity | 72 |
Is Defect Repeatative? | Yes |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | quality@sharp-engineers.com |
Plant Head/CEO Email ID | kurund.ma@sharp-engineers.com |
MD Email ID | urkhandelwal@sharp-engineers.com |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
3000
|
0
|
0
|
300
|
0
|
3300
|
Check Qty |
1500
|
0
|
0
|
300
|
0
|
1800
|
NG Qty |
72
|
0
|
0
|
0
|
0
|
72
|
Scrap | 72 |
Rework | 0 |
Under Deviation | 0 |
Containment Action |
---|
All pipe line material segregated at ETL and Sharp end |
3. Process Flow
Process Flow Description |
---|
RM incoming-Parting and drilling-CNC 1st Turning-CNC 2nd Turning-MPI inspection-plating-Final inspection-PDI- Packing and forwarding |
4. Process Details
Process / Operation | RM |
Outsource | Yes |
Machine / Cell | - |
Machine / Cell No. | - |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Method | Fixture not clean properly | Fixture clean properly also Clamping is on Across flat | O |
Method | Setting not ok | setting ok, if setting done wrong then all material will get rejected | O |
Method | Bright bar not insert properly in traub machine | Bar inserted properly also clamping is on Across flat | O |
Tool | Tool wear out | Found tool ok | O |
Material | Material grade change | Material found as per specification | O |
Material | Rae Material Condition | Raw Material found in damaged condition | X |
Machine | Parameter not set as per specification | Verified and found as per specification | O |
Man | New manpower | No new manpower | O |
Man | Unskill Manpower | Manpower available as per skill matrix | O |
Tool | Tool damaged | Found ok condition | O |
Machine | Power cut | No power cut | O |
6. Inspection Method Analysis (Current)
Inspection Method | Other |
Other Inspection Method | Visual |
Check Point at Final Inspection | Yes |
Checking Freq. | Sampling |
Sampling | No |
Sample Size | 5 |
7. Root Cause Analysis (Occurance)
Why 1 | Dent Mark-damaged |
Why 2 | Damaged at Across corner |
Why 3 | Received RM is damaged condition |
Why 4 | |
Why 5 | |
Root Cause (Occurance) | Received RM is damaged condition |
Root Cause Analysis (Outflow)
Why 1 | Dent Mark-damaged |
Why 2 | Damaged at Across corner |
Why 3 | skip from inspection |
Why 4 | inspection on sampling basis |
Why 5 | |
Root Cause (Outflow) | inspection on sampling basis |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Occurance | Started 100% Verification at incoming stage | Mr. Ravi Pande | 05/08/2024 | 05/08/2024 | Completed |
Outflow | Started 100% inspection at final inspection | Omkar Bhange | 05/08/2024 | 05/08/2024 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | Yes |
Change Details | Started 100% inspection at FI |
Inspection Method | Other |
Other Inspection Method | Visual |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100% |
10. Evidance of Countermeasure
Occurance (Before) |
Inspection on sampling basis at incoming stage 974_Occurance_Before.jpeg |
Occurance (After) |
Started 100% inspection of hex bar at incoming stage 974_Occurance_After.jpg |
Outflow (Before) |
Inspection on sampling basis 974_Outflow_Before.jpeg |
Outflow (After) |
started 100% inspection at FID with Marking 974_Outflow_After.jpeg |
11. Horizontal Deployment
Horizontal Deployment Required | No |
Applicable Machine / Model / Plant | NA |
12. Document Review
Documents | ControlPlan, PFMEA, WISOP |
Specify Other Document | NA |
13. Effectiveness Of Action
Reviewed Quantity | 50 |
Reason for submission | ok |